Accident Tingle Special N660T,
ASN logo
ASN Wikibase Occurrence # 44272
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 19 November 2005
Time:09:20
Type:Tingle Special
Owner/operator:Private
Registration: N660T
MSN: 1
Total airframe hrs:33 hours
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Tucson, AZ -   United States of America
Phase: Take off
Nature:Private
Departure airport:Tucson, AZ (57AZ)
Destination airport:Carefree, AZ (18AZ)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane entered a torque roll to the left during the initial climb shortly after takeoff. Numerous pilot witnesses observed the composite airplane on takeoff roll when the airplane began to drift to the left of centerline. Some observed dust below the left wing from the left main landing gear tire rolling in the dirt. The airplane lifted off the ground in a nose high pitch attitude and rolled 90 degrees to the left in a knife-edge turn. The airplane then continued to an inverted position, descended at a 45-degree nose low pitch attitude, and impacted the ground. All of the witnesses indicated that the engine seemed to be at full power during the entire event. Measurements of tire marks on the runway and tire tracks in the dirt to the east of the runway, indicated that the pilot continued with the takeoff roll even though the airplane was well east of the runway centerline and even departed the runway surface to the east. According to the airplane kit manufacturer, takeoffs with more than 70 percent torque were not recommended until the airplane reached 100 knots indicated airspeed. The kit manufacturer added that if one were to takeoff with more than 70-percent torque, below 100 knots, there would not be enough rudder authority to offset the torque/p-factor of the 725-horsepower engine/propeller. There was no record in the FAA database of the airplane receiving an experimental airworthiness certificate nor was there an endorsement in the logbook indicating that the pilot/builder had flown the requisite 40 hours of test flights prior to carrying passengers. The airplane was destroyed by impact and fire damage. The FAA inspector who responded to the accident site reported finding no anomalies with the identifiable components that would have prevented normal flight.
Probable Cause: The pilot's excessive use of power during takeoff, which resulted in an inadvertent torque roll shortly after lift off. Also causal was the pilot's failure to abort the takeoff when directional control could not be maintained during the takeoff roll.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX06LA041
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20051123X01883&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
06-Dec-2017 11:33 ASN Update Bot Updated [Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org