Accident Mitsubishi MU-2B-36 N103RC,
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ASN Wikibase Occurrence # 44324
 
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Date:Thursday 22 September 2005
Time:19:58
Type:Silhouette image of generic MU2 model; specific model in this crash may look slightly different    
Mitsubishi MU-2B-36
Owner/operator:Mcneely Charter Service Inc
Registration: N103RC
MSN: 673
Year of manufacture:1975
Total airframe hrs:10892 hours
Engine model:Honeywell TPE-331-6-252
Fatalities:Fatalities: 1 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:2,5 miles N of West Memphis, AR -   United States of America
Phase: Landing
Nature:Ferry/positioning
Departure airport:West Memphis, AR (AWM)
Destination airport:Gainesville, GA (GVL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The twin-engine airplane was destroyed when it impacted an earthmoving scraper and terrain in a field about 2.5 miles north of the departure airport in night visual meteorological conditions. Witnesses reported that the pilot had aborted an earlier flight when he returned to the airport and told the mechanic that he had a right engine fire warning light. The discrepancy could not be duplicated during maintenance, and the airplane departed. About 23 minutes after departure, the pilot reported to air traffic control that he needed to return to the airport to have something checked out. The pilot did not report to anyone why he decided to return to the departure airport, and he flew over four airports when he returned to the departure airport. Radar track data indicated that the airplane flew over the departure end of runway 35 at an altitude of about 1,600 feet agl, and made a descending left turn. The airplane's altitude was about 800 feet agl when it crossed the final approach course for runway 35. The airplane continued the descending left turn, but instead of landing on runway 35, the airplane flew a course that paralleled the runway, about 0.8 nm to the right of runway 35. The airplane continued to fly a northerly heading and continued to descend. The radar track data indicated that the airplane's airspeed was decreasing from about 130 kts to about 110 kts during the last one minute and fifty seconds of flight. The last reinforced beacon return indicated that the airplane's altitude was about 200 feet agl, and the airspeed was about 107 kts. The airplane impacted terrain about 0.75 nm from the last radar contact on a 338-degree magnetic heading. A witness reported that the airplane was going slow and was "extremely low." He reported that the airplane disappeared, and then there was an explosion and a fireball that went up about 1,000 feet. Inspection of the airplane revealed that it impacted the earthmover in about a wings level attitude. The landing gear handle was found to be in the landing gear UP position. The inspection of the left engine and propeller revealed damage indicative of engine operation at the time of impact. Inspection of the right engine revealed damage indicative of the engine not operating at the time of impact, consistent with an engine shutdown and a feathered propeller. No pre-existing conditions were found in either engine that would have interfered with normal operation. The inspection of the right engine fire detection loop revealed that the connector had surface contamination. When tested, an intermittent signal was produced which could give a fire alarm indication to the pilot. After the surface contamination was removed, the fire warning detection loop operated normally.
































Probable Cause: The pilot's improper in-flight decision not to land at the departure runway or other available airports during the emergency descent, and his failure to maintain clearance from a vehicle and terrain. Contributing factors were a false engine fire warning light, inadequate maintenance by company personnel, a contaminated fire warning detection loop, and night conditions.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI05FA272
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20050929X01550&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
08-Dec-2016 18:03 wf Updated [Location, Departure airport, Narrative]
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
06-Dec-2017 11:00 ASN Update Bot Updated [Operator, Departure airport, Source, Narrative]

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