ASN Wikibase Occurrence # 44881
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Date: | Tuesday 20 April 2004 |
Time: | 11:34 |
Type: | Cessna 177RG Cardinal RG |
Owner/operator: | Private |
Registration: | N1910Q |
MSN: | 177RG0310 |
Total airframe hrs: | 4269 hours |
Engine model: | Lycoming IO-360-A1B6D |
Fatalities: | Fatalities: 2 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tampa Bay, FL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Pompano Beach Airport, FL (PPM/KPMP) |
Destination airport: | Tampa-Peter O. Knight Airport, FL (TPF/KTPF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On April 20, 2004, about 1134 eastern daylight time, a Cessna 177RG, N1910Q, registered to and operated by a private individual, as a Title 14 CFR Part 91 personal flight, ditched into Tampa Bay, Tampa, Florida. Visual meteorological conditions prevailed and no flight plan was filed. The private-rated pilot and one passenger received fatal injuries, and the airplane incurred substantial damage.
An attendant at the Peter O. Knight Airport, Tampa, Florida, stated that she heard a radio communications transmission during which the voice stated that his airplane engine was experiencing roughness and backfiring. Shortly after the initial call, the attendant said she heard the pilot say "we're not going to make it." The accident airplane subsequently ditched in Tampa Bay, about a third of a mile short of the airport, in about 16 feet of water. Postaccident examination of the airplane revealed no anomalies with the airframe and flight controls or engine. During a detailed examination of the Teledyne Continental Motors dual-drive magneto, the magneto's cam was shown to have lost all lubrication, and the points were seized. Airplane records showed that the last known magneto overhaul was conducted by Electrosystems, Inc in October 1997. The records also showed that the magneto had been reinstalled on July 21, 2003, when the engine was overhauled, but a magneto overhaul had not been performed. Teledyne Continental Motors SB643B Service Bulletin pertinent to subject magneto, specifies that the magneto be overhauled when the engine is overhauled. In addition, Textron Lycoming's Mandatory Service Bulletin specifies mandatory parts replacement at overhaul and during repair and normal maintenance. Examination of the Bendix Fuel Flow Divider which was installed on the accident airplane revealed that the subject fuel flow divider did not have the latest diaphragm installation, as specified in Bendix Fuel Systems Service Bulletin RS-86, dated December 23, 1983.
Probable Cause: Improper maintenance by other maintenance personnel, and the reinstallation of an unserviced magneto during an engine overhaul, which resulted in the magneto malfunctioning, a loss of engine power, and the airplane being ditched into the water.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA04FA076 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040426X00509&key=1 Location
Images:
Photos: NTSB
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Dec-2017 17:51 |
ASN Update Bot |
Updated [Source, Narrative] |
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