ASN Wikibase Occurrence # 45063
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Date: | Friday 3 October 2003 |
Time: | 11:30 |
Type: | Bushby Mustang II |
Owner/operator: | Private |
Registration: | N888PW |
MSN: | 1699 |
Total airframe hrs: | 5 hours |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Holly Ridge, NC -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Topsail Airpark, NC (01NC) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to a witness, this was the first flight of the recently restored experimental airplane. After a brief engine run up, the airplane took off on runway 03. The takeoff appeared normal with a normal climb out. At about 300 feet above ground level, the airplane made a left turn to a wide downwind and climbed to about 800 feet or pattern altitude. After making a turn to base leg, a gradual descent was made and it seemed that he was going to make a landing on runway 03. On his turn to final he overshot the runway and lined up about 50-feet to the right of the runway. He passed over the intersection of runway 03 and 36 at an altitude of about 50 to 100 feet and added power for a go-around. The engine misfired and his increase in altitude was very slow and at the end of the runway, he started a left turn. During the turn, and at an altitude of about 100 to 200 feet, the witness thought the engine stopped. The airplane rolled to the left, nose dropped sharply and the airplane started to spin to the left. After one turn the airplane dropped out of sight behind some trees. Examination of the crash site found the airplane about 1/4 of a mile from the end of runway 36, 45-degrees left of the extended centerline in heavy trees and vegetation. Wreckage debris was scattered on a 290-degree magnetic heading. No airframe malfunctions were noted during the examination and there was nothing noted during the examination of the engine that would have prevented it from operating properly.
Probable Cause: The loss of engine power for undetermined reasons, and the pilot's failure to maintain airspeed while maneuvering for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL04LA003 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20031016X01742&key=1
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Dec-2017 19:59 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
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