ASN Wikibase Occurrence # 45256
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Date: | Wednesday 26 March 2003 |
Time: | 18:17 |
Type: | Cessna A185F |
Owner/operator: | Private |
Registration: | N53008 |
MSN: | 18502313 |
Year of manufacture: | 1974 |
Total airframe hrs: | 1754 hours |
Engine model: | Teledyne Continental IO-520-D |
Fatalities: | Fatalities: 4 / Occupants: 4 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Grand Junction, CO -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Grand Junction, CO (GJT) |
Destination airport: | Eagle, CO (EGE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The wind was from 230 to 280 at 24 knots when the pilot taxied for an intersection takeoff from runway 29. The tower controller said that during the takeoff roll, the airplane drifted off the right side of the runway and stirred up a cloud of dust. Other witnesses saw the dust cloud, but thought it was due to propeller wash or a wind gust. Immediately after liftoff, the airplane "took on a pronounced crab to the left into the wind." The pilot remarked, "Well, that was gustier than I thought, guys." The controller replied, "...looks pretty rough up there." As the airplane flew away the controller remarked, "Sure does not look like an attractive flight this evening." The pilot answered, "No, but it is time to go home." Nearby workmen said that on the evening of the accident, there was scattered rain showers of moderate intensity in the area. The airplane was found 2 days later. No discrepancies were noted during the wreckage examination. The airplane was certificated in the restricted category, and approved for "agriculture and pest control" operations. Only the two front seats were installed in the airplane. The rear two seats had been removed and were later found in the pilot's hangar. In addition to the pilot, there were three passengers aboard.
Probable Cause: the pilot's poor judgment and his failure to maintain aircraft control. Contributing factors were the high winds and downdrafts, and the pilot's self-induced pressure to go home.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DEN03FA059 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030403X00427&key=1 Location
Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Dec-2017 18:27 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
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