Accident Cessna A185F N53008,
ASN logo
ASN Wikibase Occurrence # 45256
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Wednesday 26 March 2003
Time:18:17
Type:Silhouette image of generic C185 model; specific model in this crash may look slightly different    
Cessna A185F
Owner/operator:Private
Registration: N53008
MSN: 18502313
Year of manufacture:1974
Total airframe hrs:1754 hours
Engine model:Teledyne Continental IO-520-D
Fatalities:Fatalities: 4 / Occupants: 4
Aircraft damage: Destroyed
Category:Accident
Location:Grand Junction, CO -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Private
Departure airport:Grand Junction, CO (GJT)
Destination airport:Eagle, CO (EGE)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The wind was from 230 to 280 at 24 knots when the pilot taxied for an intersection takeoff from runway 29. The tower controller said that during the takeoff roll, the airplane drifted off the right side of the runway and stirred up a cloud of dust. Other witnesses saw the dust cloud, but thought it was due to propeller wash or a wind gust. Immediately after liftoff, the airplane "took on a pronounced crab to the left into the wind." The pilot remarked, "Well, that was gustier than I thought, guys." The controller replied, "...looks pretty rough up there." As the airplane flew away the controller remarked, "Sure does not look like an attractive flight this evening." The pilot answered, "No, but it is time to go home." Nearby workmen said that on the evening of the accident, there was scattered rain showers of moderate intensity in the area. The airplane was found 2 days later. No discrepancies were noted during the wreckage examination. The airplane was certificated in the restricted category, and approved for "agriculture and pest control" operations. Only the two front seats were installed in the airplane. The rear two seats had been removed and were later found in the pilot's hangar. In addition to the pilot, there were three passengers aboard.
Probable Cause: the pilot's poor judgment and his failure to maintain aircraft control. Contributing factors were the high winds and downdrafts, and the pilot's self-induced pressure to go home.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN03FA059
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20030403X00427&key=1

Location

Revision history:

Date/timeContributorUpdates
28-Oct-2008 00:45 ASN archive Added
21-Dec-2016 19:24 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Dec-2017 18:27 ASN Update Bot Updated [Operator, Source, Narrative]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org