ASN Wikibase Occurrence # 45721
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Date: | Sunday 21 October 2001 |
Time: | 12:10 |
Type: | Stolp SA-100 Starduster |
Owner/operator: | Private |
Registration: | N64HW |
MSN: | HW101 |
Engine model: | Lycoming O-320-E |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Millstadt, IL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to witnesses to the accident, the airplane was maneuvering at a low altitude over their residence at the time of accident. The witnesses reported that the airplane was turning back towards their position when it impacted the top of a tree and subsequently impacted the terrain. One witness reported that the airplane's engine had "normal" power prior to the impact with the tree line. There was a debris field, approximately 125 feet long by 50 feet wide, which was orientated on an easterly heading. At the western edge of the debris field, approximately 125 feet from the tree line, there was a ground-impact and fragmented portions of tree material. The aircraft wreckage was located approximately 100 feet from the initial ground impact and was facing west. The entire airplane was exposed to varying degrees of fire damage. The fabric covering of the fuselage and tail surfaces were completely burned. The entire wing was consumed in the post-impact fire. The engine, cowling structure, and propeller were damaged by fire. No mechanical anomalies were found with the airplane or its flight control systems. At the pilot's last medical examination he reported that he had accumulated a total flight time of 1,500 hours.
Probable Cause: The pilot not maintaining altitude/clearance from the tree line. Factors to the accident were the pilot attempting the low altitude flight/maneuver and the presence of the tree line.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02LA007 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20011023X02138&key=1
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
28-Oct-2008 00:45 |
ASN archive |
Added |
21-Dec-2016 19:24 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
10-Dec-2017 13:13 |
ASN Update Bot |
Updated [Operator, Source, Narrative] |
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