ASN Wikibase Occurrence # 54544
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 18 December 2008 |
Time: | 03:55 |
Type: | Beechcraft 36 Bonanza |
Owner/operator: | Private |
Registration: | N7472N |
MSN: | E-32 |
Year of manufacture: | 1968 |
Total airframe hrs: | 6274 hours |
Engine model: | Continental IO 520 SERIES |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Louisville, KY -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Chicago, IL (MDW) |
Destination airport: | Louisville, KY (LOU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was cleared for the Area Navigation (RNAV) Global Positioning System (GPS) approach for runway 24 at his destine airport. The weather at the airport was reported as visibility, 6 statute miles; mist, overcast clouds at 800 feet. When the airplane was about 9 miles from the airport, the pilot reported an emergency; advising of an “engine failure”. A witness on the ground observed the airplane flying low over the golfing community. The witness reported the weather was cold, with little wind, cloudy, and misty at the time, and the street lights and a car dealership across the highway were the only illumination for the area that dark morning. The airplane was on an approximate course of 340 degrees and about a height of 30 feet above ground level (agl) when the right wing made contact with a tree at the beginning of the fairway, which was located between a row of residential homes and a row of tall trees. The right wing and the gear separated at the wheel well inboard section, the airplane contacted the ground inverted and came to rest 175 feet down the fairway from the initial contact point. Examination of the engine revealed the crankshaft and counterweight assembly was fractured through at the forward fillet radius of the number 2 main bearing journal. The number 2 main bearing journal exhibited scoring consistent with bearing rotation. The number 2 main bearings’ fragments were located in the oil sump. The number 3 main bearing journal was fractured at the rear fillet area. Examination of the crankcase halves, revealed the presence of silk thread patterns and gasket making material on the sealing surfaces of the main bearing bosses, which is not part of the engine’s manufacturer maintenance instructions that resulted in improper torque valves obtained during the crankcase halves assembly. The number 2 main bearing boss was severely damaged on both the left and right case halves. The damage included rotational mechanical gouging and deformation of the boss area behind the bearing, including mushrooming deformation of the boss. The engine was overhauled 58 hour before the accident. Witnesses reported the pilot mentioned having oil pressure problems with the overhaul engine prior to the accident.
Probable Cause: The pilot’s continued operation of the aircraft with known deficiencies. Contributing to this accident was the improper sealing of the engine case during overhaul.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09FA093 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
19-Dec-2008 23:03 |
RobertMB |
Added |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
03-Dec-2017 12:14 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
01-Oct-2020 01:04 |
Captain Adam |
Updated [Other fatalities, Location] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation