ASN Wikibase Occurrence # 58971
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Date: | Sunday 15 March 2009 |
Time: | 15:00 |
Type: | Beechcraft 24 Sierra |
Owner/operator: | Private |
Registration: | N9348S |
MSN: | MC-350 |
Total airframe hrs: | 3799 hours |
Engine model: | Lycoming IO-360-A1B6 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Corn field by Bellefontaine Municipal Airport -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Urbana, OH (I74) |
Destination airport: | Bluffton, OH (5G7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During cruise flight the pilot noticed abnormal engine noises and a partial loss of engine oil pressure. He immediately diverted to the nearest airport, but during the turn to base leg the engine oil pressure dropped to zero pounds per square inch and the engine seized. The airplane was not in a position to reach the runway threshold or to clear the airport perimeter fence. During the landing rollout the airplane impacted the airport perimeter fence, damaging both wings and the nose landing gear. An engine teardown examination revealed that the Number 3 cylinder connecting rod assembly had separated from its corresponding crankshaft journal. The journal surface was blue in color, consistent with exposure to excessive heat and lack of lubricant. The oil suction screen was obstructed with bearing material. The Number 3 cylinder connecting rod cap was found jammed beneath the counterbalance weight. One of the two connecting rod stretch bolts remained intact. The corresponding nut was found finger tight. The measured torque for the Number 2 cylinder connecting rod bolts were significantly less than the manufacturer's specification. The engine had accumulated a total of 3,799 hours since new and 492.7 hours since its last overhaul in 1999. The engine was last inspected 23.9 hours before the accident occurred.
Probable Cause: The inadequate torque of the Number 3 cylinder rod bolts by maintenance personnel, which resulted in a failure of the connecting rod and a total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN09LA209 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
17-Mar-2009 08:35 |
Digitalis |
Added |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 12:15 |
ASN Update Bot |
Updated [Cn, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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