ASN Wikibase Occurrence # 59273
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Date: | Tuesday 7 April 2009 |
Time: | 11:58 |
Type: | Grumman American AA-1B Trainer |
Owner/operator: | Private |
Registration: | N8998L |
MSN: | AA1B-0448 |
Year of manufacture: | 1974 |
Total airframe hrs: | 2295 hours |
Engine model: | Lycoming O-235-C2C |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Chesnee, South Carolina -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Landrum, SC (33A) |
Destination airport: | Landrum, SC (33A) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A witness reported that the accident airplane flew over his house and the engine sounded as if it was running slowly. The wings were rocking from side to side. As he continued to watch the airplane, the engine stopped running and the airplane descended until it crashed. The airplane impacted the ground in about a 35-degree nose-low attitude. Each wing leading edge had accordion type damage along the entire length. Examination of the fuel tanks found that they were not breached or damaged. The fuel tanks were drained; 3 gallons of fuel were recovered from the left tank and 1.5 gallons of fuel were recovered from the right tank. The recovered fuel included approximately 1 gallon from each tank that the airplane manufacturer considered unusable. The fuel selector was found in the off position. Examination of the airframe and engine did not reveal evidence of a preimpact malfunction or failure. In the month prior to the accident, the pilot was suffering from urinary symptoms that were interfering with his ability to obtain adequate sleep. Toxicology testing indicates that he had likely used at least one prescription sleep aid the night prior to the accident, in addition to relatively recent use of a sedating over-the-counter antihistamine and a prescription barbiturate medication. While the pilot’s extensive experience and the circumstances of the accident indicate the possibility that the pilot may have been distracted by physical symptoms, impaired by fatigue, or impaired by the effects of one or more of the medications he had recently ingested, the investigation was unable to determine conclusively that the pilot suffered from impairment or distraction.
Probable Cause: A loss of engine power in flight due to fuel starvation as a result of the pilot's inadequate inflight fuel planning and the pilot's failure to maintain airspeed while descending for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA09FA235 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
07-Apr-2009 13:02 |
Digitalis |
Added |
07-Apr-2009 23:07 |
slowkid |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
01-Dec-2017 18:54 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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