ASN Wikibase Occurrence # 65954
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Date: | Wednesday 24 June 2009 |
Time: | 20:41 |
Type: | Bushby Mustang II |
Owner/operator: | Private |
Registration: | N152AS |
MSN: | M-II-1688 |
Total airframe hrs: | 3 hours |
Engine model: | Lycoming (Modified) O-235-C2C |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | West Union, Ohio -
United States of America
|
Phase: | Initial climb |
Nature: | Test |
Departure airport: | West Union, OH (KAMT) |
Destination airport: | West Union, OH (KAMT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The accident occurred during an initial flight test of the experimental amateur-built airplane. On the day of the accident, the pilot was observed working on the airplane engine and completing several taxi tests before departing on the accident flight. Several witnesses reported seeing the airplane on initial climb from the runway when the engine began running rough. One witness reported seeing smoke trail from the airplane. The airplane was observed turning back toward the airport before entering a nose-down, spiraling descent until impact with the ground. A postimpact fire destroyed the fuselage cabin and cockpit. No anomalies were noted during the postaccident examination that would have resulted in the loss of engine power or the subsequent loss of airplane control. The drug Butalbital was detected in the pilot's blood and liver samples; however, the toxicological levels were significantly less than a typical therapeutic dose and would likely not have resulted in any impairment. The witness’s description of the event was consistent with the airplane entering an aerodynamic stall/spin while attempting to return to the airport after encountering a loss of engine power during initial climb.
Probable Cause: The pilot's failure to maintain adequate airspeed after a loss of engine power for undetermined reasons, which resulted in an aerodynamic stall/spin at a low altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN09LA385 |
Status: | Investigation completed |
Duration: | 2 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
25-Jun-2009 07:32 |
slowkid |
Added |
25-Jun-2009 10:45 |
slowkid |
Updated |
25-Jun-2009 10:46 |
slowkid |
Updated |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 15:37 |
ASN Update Bot |
Updated [Cn, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
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