ASN Wikibase Occurrence # 65974
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 26 June 2009 |
Time: | 09:04 |
Type: | Piper PA-32R-300 Cherokee Lance |
Owner/operator: | Propaire, Inc. |
Registration: | N38171 |
MSN: | 32R-7780392 |
Year of manufacture: | 1977 |
Total airframe hrs: | 9011 hours |
Engine model: | Lycoming IO-540-K1G5D |
Fatalities: | Fatalities: 3 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gaston´s White River Resort Airport (3M0), Arkansas -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Lakeview, AR (3MO) |
Destination airport: | St. Louis, MO (SUS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:An employee who helped load the airplane thought it was “overloaded” and that the passengers seemed “tense" and “in a hurry to leave.” The pilot made a flaps-up takeoff. It was calculated that at takeoff, the airplane was 188 pounds over maximum certificated gross weight, and the aft c.g. limit was exceeded by 0.15 inches. It was calculated that the flaps up takeoff ground roll would be approximately 1,970 feet, and the flaps up takeoff distance over a 50-foot barrier would be approximately 3,190 feet. The grass runway was 3,200 feet long. Prior to takeoff, the pilot told a surviving passenger that they were going to need all of the runway for takeoff. The passenger said the airplane lifted off at the end of the runway, dropped down into a shallow valley, touched the ground, and lifted off again. It touched down a second time, hit a barbed wire fence and tree, and “rolled” several times. Witnesses said the airplane lifted off in a nose high attitude, disappeared into a shallow valley, then reappeared in a slight climb. The wings were "wig-wagging" and the airplane was "porpoising." GPS data indicates the airplane lifted off between 74 and 78 mph and climbed no more than 29 feet. A videotape of the takeoff corroborated witness' observations. Post-accident examination of the airplane and engine did not reveal any evidence of preimpact failure or malfunction.
Probable Cause: The pilot's poor judgment/decision making in attempting the no-flap takeoff, his failure to comply with weight and balance limitations, and his failure to calculate the airplane's performance under exiting conditions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN09FA393 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Images:
(c) NTSB
(c) NTSB
Revision history:
Date/time | Contributor | Updates |
26-Jun-2009 19:11 |
slowkid |
Added |
28-Jun-2009 12:06 |
harro |
Updated |
18-Jul-2009 09:47 |
slowkid |
Updated |
05-Feb-2010 11:12 |
harro |
Updated [Time, Operator, Departure airport, Destination airport, Source, Narrative] |
05-Feb-2010 11:12 |
harro |
Updated [Departure airport] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 15:38 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation