ASN Wikibase Occurrence # 66645
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Date: | Saturday 25 July 2009 |
Time: | 11:00 |
Type: | Denney Kitfox 4 |
Owner/operator: | Private |
Registration: | N6140S |
MSN: | C9909-0253 |
Total airframe hrs: | 330 hours |
Engine model: | Rotax 912ULS |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Escondido, California -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Hemet, CA (HMT) |
Destination airport: | Ramona, CA (RNM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During cruise flight the pilot observed oil trailing along the landing gear strut. He checked the engine oil pressure indicator, and confirmed it was displaying a normal oil pressure. He then altered his flight path to include areas suitable for performing a forced landing. He continued to monitor the oil pressure as he approached an airstrip. The oil pressure did not change, and he decided to continue the flight to his destination. Shortly thereafter, the oil pressure dropped to zero, and the engine lost all power. The pilot performed a forced landing; however, during the landing roll out, the airplane struck a ditch and nosed over. Inspection of the engine revealed that the number four cylinder exhaust pushrod O-ring seal had failed, which allowed the oil to exit the engine, causing the engine to seize. The pilot stated that he had removed the cylinder head 2 years prior to the accident, and reused the exhaust pushrod O-ring seal. According to the engine manufacturer's maintenance manual recommendations, all sealing rings, gaskets, securing elements, O-rings and oil seals are to be replaced at engine reassembly.
Probable Cause: A total loss of power due to an oil exhaustion induced seizure of the engine. The pilot's decision to continue flight to the original destination after becoming aware of the in-flight oil leak instead of landing at an intermediate airport to investigate the source and extent of the problem is also causal. Contributing to the accident was the pilot's reuse of the pushrod oil seal during maintenance in contradiction to the engine manufacturer's maintenance instructions.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR09LA369 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
27-Jul-2009 09:58 |
slowkid |
Added |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
02-Dec-2017 15:49 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative, Plane category] |
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