Accident Piper PA-30-160 Twin Comanche C N8734Y,
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ASN Wikibase Occurrence # 76462
 
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Date:Monday 23 August 2010
Time:13:20
Type:Silhouette image of generic PA30 model; specific model in this crash may look slightly different    
Piper PA-30-160 Twin Comanche C
Owner/operator:Thomas B Newman
Registration: N8734Y
MSN: 30-1888
Year of manufacture:1969
Total airframe hrs:6936 hours
Engine model:Lycoming IO-360-C1C
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Near Willacoochee Highway, Douglas, Coffee County, Georgia -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Douglas, GA (DQH)
Destination airport:Douglas, GA (DQH)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane had been parked outside and not flown for about 1 year, except for a test flight conducted about 1 month prior to the accident. During a preflight inspection, the pilot observed water in the airplane's main fuel tanks, and debris in the right wingtip fuel tank. A series of engine ground run-ups and maintenance was conducted prior to the pilot attempting a test-flight. The airplane subsequently experienced a rough running left engine during the takeoff and impacted trees. Postaccident inspection of the airplane revealed the presence of water and corrosion in the fuel distribution system. Water was observed in both of the main fuel tank strainers and the left engine fuel injector. In addition, fuel drained from the airplane by recovery personnel contained water and unidentified debris. An annual inspection was performed on the airplane about 6 weeks prior to the accident, and additional maintenance was performed, which included flushing the fuel tanks and cleaning the fuel lines to each respective flow divider after the left engine "missed" during the test flight conducted about 1 month prior. The pilot had only accumulated about 22 hours of multiengine flight experience and lacked experience in the make and model of the accident airplane.
Probable Cause: A loss of engine power during takeoff due to fuel contamination. Contributing to the accident was the pilot's inadequate preflight inspection and inadequate maintenance of the fuel system.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA10LA438
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB
FAA register: 2. FAA: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=8734Y

Location

Revision history:

Date/timeContributorUpdates
24-Aug-2010 00:37 slowkid Added
24-Aug-2010 07:35 RobertMB Updated [Time, Aircraft type, Location, Departure airport, Destination airport, Source, Narrative]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
13-Apr-2017 17:48 Dr.John Smith Updated [Time, Operator, Location, Departure airport, Destination airport, Source, Narrative]
26-Nov-2017 18:07 ASN Update Bot Updated [Time, Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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