ASN Wikibase Occurrence # 78614
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Date: | Friday 8 October 2010 |
Time: | 11:45 |
Type: | Beechcraft A35 Bonanza |
Owner/operator: | Private |
Registration: | N8402A |
MSN: | D-1814 |
Year of manufacture: | 1948 |
Engine model: | Continental E225 SERIES |
Fatalities: | Fatalities: 1 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Las Vegas, Nevada -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Palm Springs, CA (PSP) |
Destination airport: | North Las Vegas, |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that, during a cross-country flight, she flew the airplane about 1.5 hours with the right fuel tank selected. When the engine lost power, she stated that she switched the fuel selector to the left and auxiliary fuel tank positions during her attempts to restart the engine, but the engine would not restart. The pilot subsequently made a forced landing on a highway, and the airplane struck a dirt embankment during the landing roll. The airplane veered to the right, and the landing gear collapsed. Postaccident examination of the engine revealed no evidence of a mechanical malfunction or failure that would have precluded normal operation. None of the fuel tanks were damaged. The right fuel tank was empty and the left tank was almost completely full (it could not be determined whether there was fuel in the auxiliary tank). After the accident, the fuel selector was found selected to the right tank position. Examination of the fuel selector confirmed that the selector switch operated normally; however, the “fuel selector not engaged” light was not functioning. The pilot should have switched tanks earlier in the flight and did not properly manage the airplane’s fuel consumption. Although the fuel selector was found in the right tank position, it could not be determined whether the pilot placed the selector in that position or if the fuel selector was not engaged when she moved it to the left and auxiliary fuel positions. Under either circumstance, the engine was starved of fuel, which resulted in a loss of engine power.
Probable Cause: The pilot’s improper fuel management, which resulted in a total loss of engine power due to fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR11LA004 |
Status: | Investigation completed |
Duration: | 1 year and 10 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
09-Oct-2010 04:34 |
Geno |
Added |
17-Nov-2010 06:20 |
gerard57 |
Updated [Total fatalities, Source, Narrative] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 18:34 |
ASN Update Bot |
Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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