ASN Wikibase Occurrence # 78788
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 17 October 2010 |
Time: | 09:00 |
Type: | SIAI-Marchetti S.205/22R |
Owner/operator: | Private |
Registration: | N934W |
MSN: | 4-181 |
Total airframe hrs: | 1905 hours |
Engine model: | Franklin 6A-350-C1 |
Fatalities: | Fatalities: 1 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Republic Airport, Long Island, NY. -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Farmingdale, NY (FRG) |
Destination airport: | Farmingdale, NY (FRG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting a low approach about 300 to 400 feet above the runway when the airplane experienced a total loss of engine power. The pilot initiated a forced landing to a road about 0.25 mile east-northeast of the departure runway. One of the passengers reported that the engine was "missing and surging" prior to the loss of engine power. A witness at the airport noted that the engine noise was smooth and steady as the airplane climbed to an altitude of about 500 to 600 feet above the ground before it suddenly sputtered and went quiet. The pilot reported that, earlier, he had aborted a takeoff due to a low cylinder temperature indication. He said that he believed that the engine may have had a fouled spark plug, which he believed had been corrected during a subsequent engine run-up. One of the passengers reported that the engine had run rough during the aborted takeoff. The airplane was maintained by the pilot and had been operated for about 17 hours since its most recent annual inspection, which was performed about 6 weeks prior to the accident. Postaccident examination of the airframe and engine, which included a carburetor flow check and examination of all spark plugs, revealed no mechanical malfunctions or failures that would have precluded normal operation.
Probable Cause: A loss of engine power during a low approach for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA11FA021 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
17-Oct-2010 16:46 |
angels one five |
Added |
17-Oct-2010 17:33 |
slowkid |
Updated [Aircraft type, Registration, Cn, Operator, Departure airport, Destination airport, Source] |
18-Oct-2010 02:15 |
chullian1819 |
Updated [Source] |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 18:36 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation