ASN Wikibase Occurrence # 335051
Date: | Monday 23 August 1954 |
Time: | 11:30 |
Type: | Douglas DC-6B |
Owner/operator: | KLM Royal Dutch Airlines |
Registration: | PH-DFO |
MSN: | 43556/257 |
Year of manufacture: | 1952 |
Total airframe hrs: | 6308 hours |
Engine model: | Pratt & Whitney R-2800 |
Fatalities: | Fatalities: 21 / Occupants: 21 |
Aircraft damage: | Destroyed, written off |
Category: | Accident |
Location: | North Sea, 37km N Dutch coast -
Netherlands
|
Phase: | En route |
Nature: | Passenger - Scheduled |
Departure airport: | Shannon Airport (SNN/EINN) |
Destination airport: | Amsterdam-Schiphol International Airport (AMS/EHAM) |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:KLM Douglas DC-6 PH-DFO (named "Willem Bontekoe") departed New York on 22 August for a flight to Amsterdam with an en-route stop at Shannon. The aircraft departed Shannon at 09:29 GMT for the last leg of the flight. After almost two hours the crew contacted Amsterdam and reported crossing the Netherlands FIR boundary. Three minutes later they contacted Amsterdam Area Control Centre reporting that they were starting the descent for Amsterdam, heading for the Spykerboor beacon. Estimated arrival time over the Spykerboor beacon was 11:37. The flight was then cleared to approach this beacon at 5500 feet or above, later amended to 4500 feet and 3500 feet or above. At 11:35 Amsterdam Area Control Centre cleared the flight to descend to 2500 feet but no answer was received. After an extensive search, hampered by low clouds, showers and heavy seas, floating debris was found at 16:10, off the Dutch coast near Bergen.
Witnesses on the ground reported having heard the flight pass overhead near Egmond (where Airway 'Green 2' crosses the coast. Other witnesses also reported seeing the aircraft at 12:01 when it passed overhead at a low altitude heading back for the sea.
Salvage work was stopped on November 25, when 45-50% of the aircraft had been brought ashore.
PROBABLE CAUSE: "A number of hypotheses as to the cause of the accident were developed. Some possibilities considered were: overheating of the electric system with heavy smoke development, explosion of one of the high pressure bottles, failure of a cockpit window failure of the automatic pilot. However, no hypothesis could be formulated in which all occurrences and evidence could be made reasonably acceptable. Therefore, in November 1955, after a 15-months' period of intensive investigation, the conclusion had to be drawn that the cause of the accident could not be established."
Sources:
ICAO Circular 50-AN/45 (p.17-19)
Location
Revision history:
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