Crash-aerien 01 DEC 1969 d'un Boeing 707-321B N892PA - Sydney-Kingsford Smith International Airport, NSW (SYD)
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Statuts:Accident investigation report completed and information captured
Date:lundi 1 décembre 1969
Heure:17:57
Type/Sous-type:Silhouette image of generic B703 model; specific model in this crash may look slightly different
Boeing 707-321B
Compagnie:Pan American World Airways (Pan Am)
Immatriculation: N892PA
Numéro de série: 20029/790
Année de Fabrication: 1969-02-20 (9 months)
Heures de vol:3044
Equipage:victimes: 0 / à bord: 11
Passagers:victimes: 0 / à bord: 125
Total:victimes: 0 / à bord: 136
Dégats de l'appareil: Substantiels
Conséquences: Repaired
Lieu de l'accident:Sydney-Kingsford Smith International Airport, NSW (SYD) (   Australie)
Phase de vol: Au décollage (TOF)
Nature:Transport de Passagers Intern.
Aéroport de départ:Sydney-Kingsford Smith International Airport, NSW (SYD/YSSY), Australie
Aéroport de destination:Honolulu International Airport, HI (HNL/PHNL), Etats-Unis d'Amérique
Numéro de vol:PA812
Détails:
PanAm flight 812, a Boeing 707, suffered a runway excursion following an aborted takeoff at Sydney Airport, Australia.
Flight 812 was departing on a nine-hour flight to Honolulu, Hawaii, USA with 125 passengers and a crew of 11.
While taxiing to the threshold of runway 34 at Sydney-Kingsford Smith International Airport, the crew completed the taxiing checklist and, in communication with Sydney Tower, received and acknowledged an airways clearance. The aircraft was initially instructed to lineup on the runway and hold but, before it had entered the runway, this instruction was changed to a take-off clearance specifying that it would be a radar departure and that, after taking off, the aircraft was to turn right onto a heading of 050 degrees and to maintain 3,000 feet. This clearance was acknowledged and the pre-take off checks were conducted as the aircraft was turning onto the runway and lining up. These checks included a gyro compass comparison which was conducted as the aircraft heading passed through 010 degrees at which time the aircraft was 34 degrees from runway alignment. At 17:57 hours flight 812 commenced its take-off from a rolling start.
The take-off was being carried out by the first officer from the right hand seat and, after the first officer had applied take-off thrust, the captain took control of the throttles while the flight engineer made fine adjustments to the throttle settings to balance the power. As the aircraft accelerated at an apparently normal rate the captain called progressively "80 knots your steering", "one hundred" and "vee one". Almost immediately after the "vee one" call the aircraft struck a flock of seagulls and there were two sharp reports from outside the aircraft. The captain observed a decay in number 2 engine EPR and aborted the take-off.
The captain stated that he applied considerable braking simultaneously with the selection of speed brake and reverse thrust and full braking almost immediately afterwards. During the early stages of the deceleration, the flight engineer saw several flickers of the anti-skid lights on the brake panel, he noted that the hydraulic pressure was normal and saw that the four reverse lights were illuminated and that the N-values on all engines was about 110% with EPR indications "well up". When the captain took control of the aircraft the first officer assisted by maintaining the nosewheel on the ground and keeping the wings level and, when reverse thrust was applied, he also placed his feet on the brakes and found that the pedals were fully depressed.
The aircraft overran the runway and struck sections of the approach lighting installation which caused the nose landing gear assembly and then the port main landing gear assembly to be removed. Finally, the nose of the aircraft came to rest partially embedded In soft ground 560 feet beyond the end of the runway and the crew and passengers then evacuated the aircraft. There were no injuries.

Probable Cause:

The probable cause of the accident was that, in the circumstances of an abandoned take-off, the aircraft could not be brought to a stop within the nominally adequate runway length because of an error in the calculation of load, a reduction in wind velocity from that forecast and the use of rolling start and braking techniques which would not ensure most effective use of the available runway length.

Accident investigation:
cover
Investigating agency: BASI
Status: Investigation completed
Duration: 243 days (8 months)
Accident number: 69-1
Download report: Final report


Photos

photo of Boeing-707-321B-N892PA
accident date: 01-12-1969
type: Boeing 707-321B
registration: N892PA
photo of Boeing-707-321B-N892PA
accident date: 01-12-1969
type: Boeing 707-321B
registration: N892PA
photo of Boeing-707-321B-N892PA
accident date: 01-12-1969
type: Boeing 707-321B
registration: N892PA
photo of Boeing-707-321B-N892PA
accident date: 01-12-1969
type: Boeing 707-321B
registration: N892PA
photo of Boeing-707-321B-N892PA
 
Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.
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