Accident McDonnell Douglas DC-10-30CF N1032F,
ASN logo
ASN Wikibase Occurrence # 329503
 

Date:Wednesday 12 November 1975
Time:13:10
Type:Silhouette image of generic DC10 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-10-30CF
Owner/operator:Overseas National Airways - ONA
Registration: N1032F
MSN: 46826/109
Year of manufacture:1973
Total airframe hrs:8193 hours
Engine model:General Electric CF6-50C
Fatalities:Fatalities: 0 / Occupants: 139
Aircraft damage: Destroyed, written off
Category:Accident
Location:New York-John F. Kennedy International Airport, NY (JFK) -   United States of America
Phase: Take off
Nature:Ferry/positioning
Departure airport:New York-John F. Kennedy International Airport, NY (JFK/KJFK)
Destination airport:Frankfurt International Airport (FRA/EDDF)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
ONA Flight 032 left the gate at 12:56 EST for a ferry flight to Jeddah via Frankfurt. The passengers were all ONA employees. The aircraft taxied to runway 13R and commenced takeoff at 13:10. Shortly after accelerating through 100 knots, but before reaching the V1 speed, a flock of birds were seen to rise from the runway. The aircraft struck many birds and the takeoff was rejected. Bird strikes had damaged the no. 3 engine's fan blades, causing rotor imbalance. Fan-booster stage blades began rubbing on the epoxy micro balloon shroud material; pulverized material then entered into the engine's HPC area, ignited and caused the compressor case to separate. A fire erupted in the right wing and no. 3 engine pylon. The aircraft couldn't be stopped on the runway. The pilot-in-command steered the aircraft off the runway onto taxiway Z at a 40 knots speed. The main undercarriage collapsed and the aircraft came to rest against the shoulder of the taxiway. The successful evacuation may be partially attributed to the fact that nearly all passengers were trained crew members.

PROBABLE CAUSE: "The disintegration and subsequent fire in the No.3 engine when it ingested a large number of seagulls. Following the disintegration of the engine, the aircraft failed to decelerate effectively because: 1) The No.3 hydraulic system was inoperative, which caused the loss of the no.2 brake system and braking torque to be reduced 50 percent; 2) the no.3 engine thrust reversers were inoperative; 3) at least three tyres disintegrated; 4) the no.3 system spoiler panels on each wing could not deploy; and 5) the runway surface was wet. The following factors contributed to the accident: 1) The bird-control program at John F. Kennedy airport did not effectively control the bird hazard on the airport; and 2) the FAA and the General Electric Company failed to consider the effects of rotor imbalance on the abradable epoxy shroud material when the engine was tested for certification."

Accident investigation:
  
Investigating agency: NTSB
Report number: DCA76AZ010
Status: Investigation completed
Duration: 1 year 1 month
Download report: Final report

Sources:

Aviation Week & Space Technology 25.07.1977 (61-63), 8.8.1977 (73-75), 15.08.1977 (61, 63, 64)
Focus on commercial aviation safety issue 19 (summer 1995)
NTSB Safety Recommendations A-76-13

Location

Images:


photo (c) NTSB; New York-John F. Kennedy International Airport, NY (JFK); November 1975; (publicdomain)


photo (c) via Werner Fischdick; New York-John F. Kennedy International Airport, NY (JFK); December 1973


photo (c) Manfred Winter; Frankfurt International Airport (FRA/EDDF); 30 July 1975


photo (c) Manfred Winter; Frankfurt International Airport (FRA/EDDF); 22 July 1974

Revision history:

Date/timeContributorUpdates

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org