Status: | Accident investigation report completed and information captured |
Date: | Wednesday 20 September 1989 |
Time: | 23:21 |
Type: |  Boeing 737-401 |
Operator: | USAir |
Registration: | N416US |
MSN: | 23884/1643 |
First flight: | 1988-12-09 (10 months) |
Total airframe hrs: | 2235 |
Cycles: | 1730 |
Engines: | 2 CFMI CFM56-3B2 |
Crew: | Fatalities: 0 / Occupants: 6 |
Passengers: | Fatalities: 2 / Occupants: 57 |
Total: | Fatalities: 2 / Occupants: 63 |
Aircraft damage: | Destroyed |
Aircraft fate: | Written off (damaged beyond repair) |
Location: | New York-La Guardia Airport, NY (LGA) ( United States of America)
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Crash site elevation: | 7 m (23 feet) amsl |
Phase: | Takeoff (TOF) |
Nature: | Domestic Scheduled Passenger |
Departure airport: | New York-La Guardia Airport, NY (LGA/KLGA), United States of America |
Destination airport: | Charlotte-Douglas Airport, NC (CLT/KCLT), United States of America |
Flightnumber: | US5050 |
Narrative:A USAir Boeing 737-401, registration N416US, was scheduled to departed from Baltimore/Washington (BWI) as flight 1846 at 15:10, but air traffic inbound to New York-LaGuardia (LGA) delayed the takeoff until 19:35. Holding on the taxiway at BWI for 1.5 hours required the flight to return to the terminal area for fuel. The Boeing 737-400 left BWI uneventfully and arrived at LGA's Gate 15 at 20:40.
Weather and air traffic in the LGA terminal area had caused cancellations and delayed most flights for several hours. The USAir dispatcher decided to cancel the Norfolk leg of Flight 1846, unload the passengers, and send the flight to Charlotte (CLT) without passengers. Several minutes later, the dispatcher told the captain that his airplane would not be flown empty but would carry passengers to Charlotte as USAir flight 5050. This seemed to upset the captain. He expressed concern for the passengers because more delays would cause him and the first officer to exceed crew duty time limitations before the end of the trip. While passengers were boarding, the captain visited USAir's ground movement control tower to ask about how decisions were made about flights and passengers.
The captain returned to the cockpit as the last of the passengers were boarding, and the entry door was closed. After the jetway was retracted, the passenger service representative told the captain through the open cockpit window that he wanted to open the door again to board more passengers. The captain refused, and flight 5050 left Gate 15 at 22:52.
The 737 taxied out to runway 31. Two minutes after push-back, the ground controller told the crew to hold short of taxiway Golf Golf. However, the captain failed to hold short of that taxiway and received modified taxi instructions from the ground controller at 22:56. The captain then briefed takeoff speeds as V1: 125 knots, VR: 128 knots, and V2: 139 knots. The first officer was to be the flying pilot. He was conducting his first nonsupervised line takeoff in a Boeing 737.
About 2 minutes later, the first officer announced "stabilizer and trim" as part of the before-takeoff checklist. The captain responded with "set" and then corrected himself by saying: "Stabilizer trim, I forgot the answer. Set for takeoff."
Flight 5050 was cleared into position to hold at the end of the runway at 23:18:26 and received takeoff clearance at 23:20:05. The first officer pressed the autothrottle disengage and then pressed the TO/GA button, but noted no throttle movement. He then advanced the throttles manually to a "rough" takeoff-power setting. The captain then said: "Okay, that's the wrong button pushed" and 9 seconds later said: "All right, I'll set your power." During the takeoff roll the airplane began tracking to the left. The captain initially used the nosewheel steering tiller to maintain directional control. About 18 seconds after beginning the roll a "bang" was heard followed shortly by a loud rumble, which was due to the cocked nosewheel as a result of using the nosewheel steering during the takeoff roll. At 23:20:53, the captain said "got the steering." The captain later testified that he had said, "You've got the steering." The first officer testified that he thought the captain had said: "I've got the steering." When the first officer heard the captain, he said "Watch it then" and began releasing force on the right rudder pedal but kept his hands on the yoke in anticipation of the V1 and rotation callouts.
At 23:20:58.1, the captain said: "Let's take it back then" which he later testified meant that he was aborting the takeoff. According to the captain, he rejected the takeoff because of the continuing left drift and the rumbling noise. He used differential braking and nose wheel steering to return toward the centerline and stop. The throttle levers were brought back to their idle stops at 23:20:58.4. The indicated airspeed at that time was 130 knots. Increasing engine sound indicating employment of reverse thrust was heard on the CVR almost 9 seconds after the abort maneuver began. The airplane did not stop on the runway but crossed the end of the runway at 34 knots ground speed. The aircraft dropped onto the wooden approach light pier, which collapsed causing the aircraft break in three and drop into 7-12 m deep East River. The accident was not survivable for the occupants of seats 21A and 21B because of the massive upward crush of the cabin floor.
Probable Cause:
PROBABLE CAUSE: "The captain's failure to exercise his command authority in a timely manner to reject the take-off or take sufficient control to continue the take-off, which was initiated with a mistrimmed rudder. Also causal was the captain's failure to detect the mistrimmed rudder before the take-off was attempted."
Board member Jim Burnett filed the following concurring and dissenting statement: "Although I concur with the probable cause as adopted as far as it goes, I would have added the following as a contributing factor: Contributing to the cause of the accident was the failure of USAir to provide an adequately experienced and seasoned flight crew."
Accident investigation:
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Investigating agency: | NTSB  |
Status: | Investigation completed |
Duration: | 286 days (10 months) | Accident number: | NTSB/AAR-90-03 | Download report: | Final report
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Classification:
Wrong takeoff configuration (flaps/trim)
Rejected takeoff
Runway excursion
Sources:
» Aviation Week & Space Technology 2 October 1989 (32,33)
» NTSB/AAR-90/03
Follow-up / safety actions
FAA issued 1 Airworthiness Directive
NTSB issued 6 Safety Recommendations
Issued: 06-AUG-1990 | To: Boeing 737-400,-400 | AD 90-14-02 |
Replace the rudder trim control knob with a smooth rounded fluted knob, to prevent inadvertent rudder trim resulting in unacceptably increasing the level of pilot effort required to maintain the correct heading during takeoff |
Issued: 03-SEP-1990 | To: FAA | A-90-104 |
DEVELOP STANDARDS FOR THE DESIGN, CONSTRUCTION, OPERATION, AND PERFORMANCE OF MEGAPHONES. (Closed - Acceptable Action) |
Issued: 03-SEP-1990 | To: FAA | A-90-105 |
REQUIRE AIRLINES TO PROVIDE AIRPORT CRASH/FIRE RESCUE PERSONNEL ACCURATE AND TIMELY NUMBERS OF ALL PERSONS ABOARD AN ACCIDENT/INCIDENT AIRCRAFT, AND TO PROVIDE ASSISTANCE IN DETERMINING THE DISPOSITION OF PERSONS WHO HAVE BEEN RE COVERED FROM THE SCENE OF AN ACCIDENT. (Closed - Acceptable Action) |
Issued: 03-SEP-1990 | To: FAA | A-90-106 |
REQUIRE AIR CARRIERS TO ADOPT PROCEDURES THAT WOULD RESULT IN THE COMPLETION OF A MODIFIED OR FULL ACCEPTANCE CHECKLIST WHENEVER THE FLIGHTCREW HAS VACATED THE COCKPIT. (Closed - Acceptable Alternate Action) |
Issued: 03-SEP-1990 | To: FAA | A-90-107 |
ISSUE AN AIR CARRIER OPERATIONS BULLETIN DIRECTING ALL PRINCIPAL OPERATIONS INSPECTORS TO URGE AIR CARRIERS TO SCHEDULE NEWLY TRAINED CAPTAINS AND FIRST OFFICERS ON REGULAR TRIP SCHEDULES IMMEDIATELY FOLLOWING COMPLETION OF TRAINING, UNTIL THEY ACCRUE A PRESCRIBED AMOUNT OF LINE OPERATING TIME IN THEIR RESPECTIVE POSITIONS IN ORDER TO CONSOLIDATE THEIR RECENTLY-ACQUIRED TRAINING. (Closed - Acceptable Action) |
Issued: 03-SEP-1990 | To: FAA | A-90-108 |
AMEND 14 CFR 121.385 TO SPECIFY A COMBINED EXPERIENCE LEVEL FOR INITIAL PILOT-IN-COMMAND AND INITIAL SECOND-IN COMMAND PILOTS WHICH WOULD PRECLUDE THE PAIRING OF TWO PILOTS, EACH OF WHOM HAS RELATIVELY LOW EXPERIENCE IN HIS OR HER RESPECTIVE POSITION. (Closed - Acceptable Action) |
Issued: 03-SEP-1990 | To: Port Authority of New York and New Jersey | A-90-111 |
SURVEY THE 1,000 FOOT BY 500 FOOT SURFACE AREA CONTIGUOUS TO THE DEPARTURE ENDS OF THE RUNWAYS AT THE LAGUARDIA AIRPORT IN ORDER TO MINIMIZE HAZARDS TO AIRPLANES THAT DO NOT STOP ON THE RUNWAYS. (Closed - Acceptable Action) |
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Photos

accident date:
20-09-1989type: Boeing 737-401
registration: N416US

accident date:
20-09-1989type: Boeing 737-401
registration: N416US

accident date:
20-09-1989type: Boeing 737-401
registration: N416US
Map
This map shows the airport of departure and the intended destination of the flight. The line between the airports does
not display the exact flight path.
Distance from New York-La Guardia Airport, NY to Charlotte-Douglas Airport, NC as the crow flies is 869 km (543 miles).
Accident location: Approximate; accuracy within a few kilometers.
This information is not presented as the Flight Safety Foundation or the Aviation Safety Network’s opinion as to the cause of the accident. It is preliminary and is based on the facts as they are known at this time.