Status: | Accident investigation report completed and information captured |
Datum: | Freitag 27 Dezember 1991 |
Zeit: | 08:51 |
Flugzeugtyp: | McDonnell Douglas DC-9-81 (MD-81) |
Fluggesellschaft: | Scandinavian Airlines System - SAS |
Kennzeichen: | OY-KHO |
Werknummer: | 53003/1844 |
Baujahr: | 1991 |
Betriebsstunden: | 1608 |
Anzahl Zyklen der Zelle: | 1272 |
Triebwerk: | 2 Pratt & Whitney JT8D-217C |
Besatzung: | Todesopfer: 0 / Insassen: 7 |
Fluggäste: | Todesopfer: 0 / Insassen: 122 |
Gesamt: | Todesopfer: 0 / Insassen: 129 |
Sachschaden: | Zerstört |
Konsequenzen: | Written off (damaged beyond repair) |
Unfallort: | nahe Gottröra ( Schweden)
|
Flugphase: | Anfangssteigflug (ICL) |
Betriebsart: | Internationaler Linienflug |
Flug von: | Stockholm-Arlanda Airport (ARN/ESSA), Schweden |
Flug nach: | København-Kastrup Airport (CPH/EKCH), Dänemark |
Flugnummer: | SK751 |
Unfallbericht:The MD-81 arrived from Zurich at 22:09 and was parked at gate 2 overnight with temperatures of around +1 deg. C. Approx. 2550 kg of fuel remained in each wing tank. The aircraft was scheduled to leave Stockholm for Copenhagen at 08:30 and the temperature had dropped to -0 deg C in the early morning. During the night and in the early morning clear ice had formed on the upper side of the wings, but this was not detected by the ground crew member who checked the forward part of the wing. The aircraft was fuelled with 1400 kg of fuel and was ready for de-icing at 08:30, which was done using 850l of Type I fluid. After de-icing the mechanic didn't check whether there was any clear ice on the upper side of the wings, since he had previously found none. The flight was then cleared to taxi to runway 08 and the aircraft took off at 08:47. After 25 seconds (at 1124 feet height) bangs, vibrations and jerks were perceived in the aircraft. This was caused by a no. 2 engine surge. The engine was throttled down a little, but throttle control simultaneously changed to an automatic mode which increased throttle setting with altitude (Automatic Thrust Restoration - ATR). This in turn increased the intensity of the surging. The no. 1 engine surged 39 seconds later, but this was not noticed by the flight crew. An attempt to switch on the autopilot at 2616 feet failed. At 76 resp. 78 seconds into the flight both the no. 2 and no. 1 engine failed after breakup of the stage 1 stators of both engines (initiated by high loads from the surges). The aircraft was climbing through 3206 feet at that moment with a 196 KIAS. A no. 1 engine fire warning at 91 seconds into the flight made the crew activate the fire extinguishing system. A SAS captain traveling the passenger cabin realized that there were problems and hurried to the cockpit to assist the flight crew. The aircraft was in a gliding left turn at that moment. When descending through 420 m, still in the clouds, the assisting captain gradually extended the flaps. The flaps were fully extended at 1100 feet (340 m) and the plane broke through the clouds at 980-820 feet. A field in the direction of flight was chosen for an emergency landing. The wheels were selected down and Stockholm control was informed about the imminent crash-landing. The MD-81 contacted trees at 121 knots and a major portion of the right wing broke off. The plane then struck sloping ground tail-first and slid along the ground for 110 m. The fuselage was broken into three pieces, but there was no fire.
Probable Cause:
CAUSES OF THE ACCIDENT: "The accident was caused by SAS' instructions and routines being inadequate to ensure that clear ice was removed from the wings of the aircraft prior to takeoff. Hence the aircraft took off with clear ice on the wings. In connection with lift-off, the clear ice loosened and was ingested by the engines. The ice caused damage to the engine fan stages, which led to engine surges. The surges destroyed the engines.
Contributory causes were: The pilots were not trained to identify and eliminate engine surging; ATR-which was unknown within SAS - was activated and increased the engine power without the pilot's knowledge."
Accident investigation:
|
Investigating agency: | SHK Sweden |
Status: | Investigation completed |
Duration: | 1 year and 10 months | Accident number: | SHK C1993:57 | Download report: | Final report
|
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Informationsquelle:
»
SKYbrary » Air Safety Week 1 November 1993 (p. 1,2)
» ICAO Adrep Summary 2/92 (#16)
» ICAO Adrep Summary 2/94 (#19)
» NRC Handelsblad 27.12.1991
» NTSB Safety Recommendations A-92-11 through -15
» Scramble 152
Sicherheitsempfehlungen
NTSB issued 5 Safety Recommendations
Issued: 18-MAR-1992 | To: FAA | A-92-11 |
REQUIRE THAT OVERHEAD STOWAGE BINS MANUFACTURED BY C&D INTERIORS AND INSTALLED IN MD-80 SERIES AIRPLANES BE MODIFIED TO ENSURE THAT THE BINS REMAIN SECURED TO THEIR ANCHORAGES, THE BIN DOORS REMAIN CLOSED, AND THAT PASSENGER SERVICE UNITS REMAIN ATTACHED TO THE BINS DURING ACCIDENTS IN WHICH SURVIVABLE LOADS ARE APPLIED TO THE THREE MAJOR AXES IN COMBINATION. (Closed - Unacceptable Action) |
Issued: 18-MAR-1992 | To: FAA | A-92-12 |
REVIEW THE DESIGN OF THE C&D INTERIORS OVERHEAD STOWAGE BINS THAT ARE INSTALLED IN AIRPLANES OTHER THAN THE MD-80, AND ORDER ANY CORRECTIVE ACTION THAT MAY BE REQUIRED, AS CITED IN (A-92-11). (Closed - Unacceptable Action) |
Issued: 18-MAR-1992 | To: FAA | A-92-13 |
AMEND THE APPROPRIATE SUBPARTS OF 14 CFR 25.561 TO ESTABLISH AND REQUIRE DYNAMIC TESTING STANDARDS FOR OVERHEAD STOWAGE BINS AND ALL BIN COMPONENT FIXTURES. (Closed - Unacceptable Action) |
Issued: 18-MAR-1992 | To: FAA | A-92-14 |
REQUIRE THAT TRANSPORT CATEGORY AIRPLANES MANUFACTURED AFTER A CERTAIN DATE BE EQUIPPED WITH OVERHEAD STOWAGE BINS AND COMPONENT FIXTURES THAT MEET THE REQUIREMENTS OF DYNAMIC TEST STANDARDS. (Closed - Unacceptable Action) |
Issued: 18-MAR-1992 | To: FAA | A-92-15 |
DEVELOP A TIMETABLE THAT WILL REQUIRE THE MODIFICATION OF ALL BINS AND COMPONENT FIXTURES CURRENTLY IN SERVICE ON TRANSPORT CATEGORY AIRPLANES IN ORDER TO MEET THE NEW DYNAMIC TESTS STANDARDS AS CITED IN A-92-13. (Closed - Unacceptable Action) |
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Fotos
accident date:
27-12-1991type: McDonnell Douglas MD-81
registration: OY-KHO
accident date:
27-12-1991type: McDonnell Douglas MD-81
registration: OY-KHO
accident date:
27-12-1991type: McDonnell Douglas MD-81
registration: OY-KHO
Map
This map shows the airport of departure and the intended destination of the flight. The line between the airports does
not display the exact flight path.
Distance from Stockholm-Arlanda Airport to København-Kastrup Airport as the crow flies is 543 km (339 miles).
Accident location: Approximate; accuracy within a few kilometers.
This information is not presented as the Flight Safety Foundation or the Aviation Safety Network’s opinion as to the cause of the accident. It is preliminary and is based on the facts as they are known at this time.