Vliegtuigongeval op 26 JUL 1993 met Canadair CL-600-2B19 Regional Jet CRJ-100 C-FCRJ - Byers, KS
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Status:Accident investigation report completed and information captured
Datum:maandag 26 juli 1993
Tijd:13:52
Type:Silhouette image of generic CRJ1 model; specific model in this crash may look slightly different
Canadair CL-600-2B19 Regional Jet CRJ-100
Luchtvaartmaatschappij:Bombardier Aerospace
Registratie: C-FCRJ
Constructienummer: 7001
Bouwjaar: 1991
Aantal vlieguren:771
Aantal vluchten:800
Bemanning:slachtoffers: 3 / inzittenden: 3
Passagiers:slachtoffers: 0 / inzittenden: 0
Totaal:slachtoffers: 3 / inzittenden: 3
Schade: Vernield
Gevolgen: Written off (damaged beyond repair)
Plaats:Byers, KS (   Verenigde Staten)
Fase: Manoeuvreren (MNV)
Soort vlucht:Test
Vliegveld van vertrek:Wichita-Mid-Continent Airport, KS (ICT/KICT), Verenigde Staten
Vliegveld van aankomst:Wichita-Mid-Continent Airport, KS (ICT/KICT), Verenigde Staten
Beschrijving:
The Canadair plane was on a test flight out of Wichita, KS to evaluate flying qualities in a new 8deg. takeoff flap setting and to demonstrate compliance with US 14 CFR 25:177 rules. The aircraft lost control during a low speed steady-heading sideslip test manoeuvre at FL120. The crew were to end a Steady Heading Sideslip (SHSS) manoeuvre at a 15deg sideslip, but continued to 21deg. at full rudder. The plane rolled rapidly through 360deg and entered a deep stall. As it descended through 8000 feet the captain requested the co-pilot to deploy the anti-spin parachute, which he complied with. The co-pilot however, didn't close the jaws (which connect/disconnect the parachute from the airplane) before chute deployment. The chute thus fell free of the plane. Control was not regained and the aircraft crashed and skidded for about 200 yards through several cornfields.

Probable Cause:

PROBABLE CAUSE: "The captain's failure to adhere to the agreed upon flight test plan for ending the test manoeuvre at the onset of prestall stick shaker, and the flight crew's failure to assure that all required switches were properly positioned for anti-spin chute deployment. A factor which contributed to the accident was the inadequate design of the anti-spin chute system which allowed deployment of the chute with the hydraulic lock switch in the unlocked position. (When in the unlocked position, the hooks clasping the chute shackle to the airframe are open.)"

Accident investigation:

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Investigating agency: NTSB
Status: Investigation completed
Duration: 277 days (9 months)
Accident number: CHI93MA276
Download report: Final report

Bronnen:
» Air International September 1993, p.127
» Aviation Week & Space Technology 02.08.1993 (39-40)
» NTSB Safety Recommendation A-94-101
» Scramble 170


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This information is not presented as the Flight Safety Foundation or the Aviation Safety Network’s opinion as to the cause of the accident. It is preliminary and is based on the facts as they are known at this time.
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CRJ100

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