Crash-aerien 14 MAR 1997 d'un McDonnell Douglas MD-87 N753RA - Detroit-Metropolitan Wayne County Airport, MI (DTW)
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Statuts:Accident investigation report completed and information captured
Date:vendredi 14 mars 1997
Heure:06:47
Type/Sous-type:Silhouette image of generic MD87 model; specific model in this crash may look slightly different
McDonnell Douglas MD-87
Compagnie:Reno Air
Immatriculation: N753RA
Numéro de série: 49587/1541
Année de Fabrication: 1988
Moteurs: 2 Pratt & Whitney JT8D-219
Equipage:victimes: 0 / à bord: 5
Passagers:victimes: 0 / à bord: 106
Total:victimes: 0 / à bord: 111
Dégats de l'appareil: Substantiels
Conséquences: Repaired
Lieu de l'accident:Detroit-Metropolitan Wayne County Airport, MI (DTW) (   Etats-Unis d'Amérique)
Phase de vol: Au décollage (TOF)
Nature:Transport de Passagers Nat.
Aéroport de départ:Detroit-Metropolitan Wayne County Airport, MI (DTW/KDTW), Etats-Unis d'Amérique
Aéroport de destination:Reno/Tahoe International Airport, NV (RNO/KRNO), Etats-Unis d'Amérique
Numéro de vol: 153
Détails:
A McDonnell Douglas MD-87, N753RA, operated as Reno Air flight 153 from Detroit, Michigan, to Reno, Nevada, experienced a partial loss of power on both engines during takeoff. The flight returned to Detroit and landed at 06:58 without further incident. Neither the 5 crewmembers nor the 106 passengers were injured.
The captain stated that he was aware that there had been an ice storm during the night prior to the accident. The first officer reported that during the preflight he noted a layer of frost on the bottom of the right wing. He also reported that he used a ladder to inspect the top of both wings using the "stick" and his hand. He did not find any ice. In addition, after entering the cockpit he went outside once again and inspected the right wing for ice, using the stick and his hand. Once again, he did not detect any ice. According to the captain, he went into the cabin area and looked out the windows at the wings as the first officer was outside. He said the wings were wet, but there was no ice. At 06:00 EST, the captain informed the ground crew that the airplane would not need to be deiced.
The captain reported they were pushed back from the gate at 06:35 and began taxiing at 06:37. At 06:45 the airplane taxied onto runway 03L for takeoff. The captain reported he held the brakes and ran the engines to 1.4 engine pressure ratio (EPR) which was about 70% N1. He reported all engine indications were normal so he stabilized the engines at 1.6 EPR. The captain then called for autothrottles ON and the power increased to 2.02 EPR. The first officer stated that the airspeed seemed to stagnate for "a second" at 100 knots during the takeoff roll. He said he called V1 a little slower than normal and the captain rotated slightly slower than normal.
Both pilots reported the first indication of a problem occurred immediately after liftoff at an altitude of 50 to 100 feet above the ground. The captain reported the "right engine popped" and the No.1 engine EPR gauge fluctuated. The first officer reported hearing a loud popping sound and the airplane shuddered.
The pilots reported that they received clearance from the tower to land on any runway. The captain said he disengaged the autothrottles and pulled the left throttle back a half knob behind the right throttle because the left engine seemed more erratic. The captain then called for gear retraction.

The captain reported that at an altitude of about 200 agl the airspeed decreased to approximately V2 and the airplane had very little climb performance. They advanced the left throttle so it was even with the right and once the gear was retracted the rate of climb increased. The captain reported the EPRs were fluctuating above 2.02.
The crew reported they initially turned the airplane for a landing on runway 21L. The flaps remained extended 11 degrees and both engines were experiencing compressor stalls. The captain reported they climbed to an altitude of 3,400 feet mean sea level (msl). The crew completed the appropriate checklists and were cleared to descend to 3,000 feet msl. The first officer suggested they turn on the airfoil anti-ice system as the captain reduced the power to descend. The captain reported that when power on the engines was reduced through an EPR setting of 1.60 to 1.70 and the airspeed decreased to approximately 180 knots, the compressor stalls stopped. The crew elected to change runways to land on runway 3L due to weight conditions and runway length. The airplane landed without incident.

Probable Cause:

PROBABLE CAUSE: "The captains failure to have the airplane deiced prior to takeoff which resulted in ice ingestion into both engines. Factors associated with the accident were the icing weather conditions, wing ice, an inadequate detection of the ice during the preflight, and the dark lighting conditions when the first officer was performing the preflight."

Accident investigation:

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Investigating agency: NTSB
Status: Investigation completed
Duration: 3 years
Accident number: CHI97FA083
Download report: Summary report

Sources:
» NTSB


Opérations de secours

NTSB issued 2 Safety Recommendations

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Plan
Ce plan montre l'aéroport de départ ainsi que la supposée destination du vol. La ligne fixe reliant les deux aéroports n'est pas le plan de vol exact.
La distance entre Detroit-Metropolitan Wayne County Airport, MI et Reno/Tahoe International Airport, NV est de 3033 km (1896 miles).

Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.
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