ASN Wikibase Occurrence # 323728
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Date: | Monday 14 June 1999 |
Time: | 10:38 |
Type: | Beechcraft A100 King Air |
Owner/operator: | Thunder Airlines |
Registration: | C-GASW |
MSN: | B-108 |
Year of manufacture: | 1972 |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Destroyed, written off |
Category: | Accident |
Location: | Thunder Bay Airport, ON (YQT) -
Canada
|
Phase: | Take off |
Nature: | Passenger - Non-Scheduled/charter/Air Taxi |
Departure airport: | Thunder Bay Airport, ON (YQT/CYQT) |
Destination airport: | Red Lake Airport, ON (YRL/CYRL) |
Investigating agency: | TSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Thunder Airlines Beechcraft A100 King Air took off at 10:34 on a charter flight from Thunder Bay Airport, ON (YQT), for Red Lake Airport, ON (YRL), with two pilots and three passengers on board. After getting airborne, the aircraft pitched up to approximately 70 degrees, reaching a height estimated to be between 500 and 700 feet above ground level. It then rolled to the left, pitched steeply nose-down, and descended to the ground within the confines of the airport. The aircraft contacted the soft, level ground in a relatively level attitude and covered a distance of about 500 feet before coming to rest in a wooded area immediately beyond an elevated railroad bed and track. The cabin remained intact during the crash sequence, and all occupants escaped without any injuries. The aircraft was damaged beyond repair. An ensuing fuel-fed fire was rapidly extinguished by airport emergency response services (ERS) personnel.
Causes and Contributing Factors:
The flight crew lost pitch control of the aircraft on take-off when the stabilizer trim actuators became disconnected because they had not been properly reinstalled by the AME during maintenance work conducted before the flight. The crew chief responsible for the inspection did not ensure correct assembly of the stabilizer trim actuators, which contributed to the accident.
Accident investigation:
|
| |
Investigating agency: | TSB |
Report number: | A99H0002 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
Location
Revision history:
Date/time | Contributor | Updates |
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