ASN Wikibase Occurrence # 323365
Date: | Thursday 4 January 2001 |
Time: | 15:47 |
Type: | Learjet 35 |
Owner/operator: | Air Response North |
Registration: | N435JL |
MSN: | 35-018 |
Year of manufacture: | 1975 |
Total airframe hrs: | 16302 hours |
Engine model: | Garrett TFE731 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial, written off |
Category: | Accident |
Location: | Schenectady-County Airport, NY (SCH) -
United States of America
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Phase: | Take off |
Nature: | Ambulance |
Departure airport: | Schenectady-County Airport, NY (SCH/KSCH) |
Destination airport: | New York-La Guardia Airport, NY (LGA/KLGA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Learjet 35, N435JL, was substantially damaged during an aborted takeoff at the Schenectady-County Airport, NY (SCH). The certificated airline transport pilot, commercial pilot, and passenger were not injured. Visual meteorological conditions prevailed, and an IFR flight plan was filed for the air response medical flight to New York-La Guardia Airport, NY (LGA).
The captain stated that prior to departure the flight controls were tested, with no abnormalities noted, and the takeoff trim was set to the "middle of the takeoff range," without referring to any available pitch trim charts. During the takeoff roll on runway 28, the pilot attempted to rotate the airplane twice, and then aborted the takeoff halfway down the 4,840 foot long runway, because the controls "didn't feel right." The airplane traveled off the departure end of the runway and through a fence, and came to rest near a road. The pilot reported no particular malfunction with the airplane. Examination of the airplane revealed that the horizontal stabilizer was positioned at -4.6 degrees, the maximum nose down limit within the takeoff range. The horizontal stabilizer trim and elevator controls were checked, and moved freely through their full ranges of travel. According to the AFM TAKEOFF TRIM C.G. FUNCTION chart, a horizontal stabilizer trim setting of -7.2 was appropriate with the calculated C.G. of 20% MAC.
PROBABLE CAUSE: "The pilot's improper trim setting, which resulted in a runway overrun and impact with a fence."
Accident investigation:
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Investigating agency: | NTSB |
Report number: | IAD01LA022 |
Status: | Investigation completed |
Duration: | 1 year and 8 months |
Download report: | Final report |
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Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
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