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Date: | Wednesday 15 June 2011 |
Time: | 17:25 |
Type: | Cessna 525A CitationJet CJ2 |
Owner/operator: | Deer Horn Aviation |
Registration: | N129SG |
MSN: | 525A0129 |
Year of manufacture: | 2002 |
Total airframe hrs: | 3224 hours |
Engine model: | Williams International FJ44 |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial, repaired |
Category: | Accident |
Location: | Nashville-John C. Tune Airport, TN -
United States of America
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Phase: | Landing |
Nature: | Executive |
Departure airport: | Artesia Airport, NM (ATS/KATS) |
Destination airport: | Nashville-John C. Tune Airport, TN (KJWN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Cessna 525A, N129SG, was substantially damaged following a runway overrun at Nashville-John C. Tune Airport, Tennessee, USA. The pilot and four passengers were not injured.
The pilot-in-command (PIC) was in the left cockpit seat, and a passenger, who possessed a student pilot certificate, was in the right cockpit seat. The PIC was not a certificated flight instructor; however, the student pilot was at the controls for a majority of the flight. During the descent and initial approach, the student pilot allowed the airplane to become high and fast, and the PIC subsequently took over the controls and continued the approach. During the final approach, the ground proximity warning system announced "sink rate" eight times. After touchdown, the antiskid system activated; however, there was insufficient runway remaining on which to stop the airplane. The PIC reported that he neglected to consider the wet runway condition. The airplane overran the runway and struck the instrument landing system antennas before coming to a stop. The PIC reported that there were no mechanical malfunctions or failures during the flight. As a result of the accident, the operator modified its operational procedures to restrict unqualified personnel from the cockpit during flight and initiated a formal risk assessment program.
Probable Cause: The pilot-in-command's failure to execute a go-around when the airplane was high and fast on the final approach.
Accident investigation:
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Investigating agency: | NTSB |
Report number: | ERA11LA345 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
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Sources:
Location
Images:
photo (c) NTSB; Nashville-John C. Tune Airport, TN; 15 June 2011
photo (c) NTSB; Nashville-John C. Tune Airport, TN; 15 June 2011
Revision history:
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