Statuts: | Accident investigation report completed and information captured |
Date: | vendredi 8 décembre 2017 |
Heure: | 10:17 |
Type/Sous-type: | GAF Nomad N.22C |
Compagnie: | Bayswater Road Ltd. |
Immatriculation: | VH-ATO |
Numéro de série: | 108 |
Année de Fabrication: | 1979 |
Heures de vol: | 11053 |
Moteurs: | 2 Allison 250-B17C |
Equipage: | victimes: 0 / Ã bord: 1 |
Passagers: | victimes: 0 / Ã bord: 0 |
Total: | victimes: 0 / Ã bord: 1 |
Dégats de l'appareil: | Substantiels |
Lieu de l'accident: | Buka Airport (BUA) ( Papouasie Nouvelle-Guinée)
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Phase de vol: | A l'atterrissage (LDG) |
Nature: | Surveillance |
Aéroport de départ: | Buka Airport (BUA/AYBK), Papouasie Nouvelle-Guinée |
Aéroport de destination: | Buka Airport (BUA/AYBK), Papouasie Nouvelle-Guinée |
Détails:The GAF Nomad aircraft, registered VH-ATO, owned and operated by Bayswater Road Ltd, departed Buka Airport, conducting an aerial survey under VFR. The pilot-in-command was the sole occupant.
The pilot reported that when doing the pre-landing checks the landing gear failed to extend. He attempted to deploy the landing gear using the emergency system (which consists in a manual pump), but the handle of the manual pump broke after three to four pumps. The pilot decided to perform a landing in the grassy flight strip, which was about 32 metres to the right of the sealed runway centerline.
There was significant damage to both landing-gear pods and the nose forward of the nose locker. The landing gear doors had significant skin damage and were not aligned with the pods. The nose cone was punctured and torn on the underside. The lower attachment points of both wingsÂ’ struts came into contact with the landing-gear pods and fracturing the pods side skins. The trailing skin on the left lower strut was bent.
Probable Cause:
AIC comment:
The landing gear system was examined including the electrical wiring. The wire to the up-lock switch on the right land gear had fractured and separated, rendering the normal landing gear extension system inoperative.
Excessive force due to the resistance of the locked-up landing gear extension motor during the pumping to extend the gear manually, likely contributed to the overload failure of the handle.
Accident investigation:

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Investigating agency: | AIC PNG |
Status: | Investigation completed |
Duration: | 146 days (5 months) | Accident number: | AIC 17-1003 | Download report: | Final report
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Photos
accident date:
08-12-2017type: GAF Nomad N.22C
registration: VH-ATO
accident date:
08-12-2017type: GAF Nomad N.22C
registration: VH-ATO
Plan
Les informations ci-dessus ne représentent pas l'opinion de la 'Flight Safety Foundation' ou de 'Aviation Safety Network' sur les causes de l'accident. Ces informations prélimimaires sont basées sur les faits tel qu'ils sont connus à ce jour.