Date: | Saturday 13 February 2021 |
Time: | 11:40 |
Type: | Dassault Falcon 900EX EASy |
Owner/operator: | Aerospike Iron LLC |
Registration: | N823RC |
MSN: | 201 |
Year of manufacture: | 2008 |
Total airframe hrs: | 2914 hours |
Engine model: | Honeywell TFE731-60-1C |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial, written off |
Category: | Accident |
Location: | San Diego-Montgomery-Gibbs Executive Airport, CA (MYF) -
United States of America
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Phase: | Take off |
Nature: | Private |
Departure airport: | San Diego-Montgomery-Gibbs Executive Airport, CA (MYF/KMYF) |
Destination airport: | Kona-Keahole Airport, HI (KOA/PHKO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:A Dassault Falcon 900EX corporate jet, registration N823RC, experienced a landing gear collapse subsequent to an aborted takeoff attempt from runway 28R at Montgomery-Gibbs Exec Airport (MYF/KMYF), San Diego, California.
The airplane sustained substantial damage and the five occupants onboard were not injured.
The flight crew later stated that at rotation speed, the captain applied back pressure to the control yoke; however, the nose did not rotate to a takeoff attitude. The captain attempted to rotate the airplane once more by relaxing the yoke then pulling it back again, and, with no change in the airplanes attitude, he made the decision to reject the takeoff by retarding the thrust levers and applying maximum braking. The airplane overran the end of the runway onto a gravel pad where the landing gear collapsed.
The NTSB reported that the captain did not have a valid pilot certificate. A review of airmen records revealed that the FAA had
issued an emergency revocation of all his certificates 2 years earlier on February 13, 2019.
FAA records indicated that the reason for the emergency revocation was because he had falsified logbook entries and records for pilot proficiency checks, competency checks, and training events on 15 separate occasions while employed as a check pilot for a Part 135 operator.
Probable Cause: The flight crews operation of the airplane outside of the manufacturers specified weight and balance limitations and with an improper trim setting, which resulted in the airplanes inability to rotate during the attempted takeoff. Contributing to the accident, was the captains lack of proper certification and the crews lack of flight experience in the airplane make and model.
Accident investigation:
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Investigating agency: | NTSB |
Report number: | WPR21LA110 |
Status: | Investigation completed |
Duration: | 2 years and 3 months |
Download report: | Final report |
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Sources:
https://www.nbcsandiego.com/news/local/corporate-jet-goes-off-runway-at-montgomery-airport-in-kearny-mesa/2521094/ https://www.sandiegouniontribune.com/news/public-safety/story/2021-02-13/plane-crashes-during-takeoff-at-montgomery-field-airport Location
Images:
photo (c) daviator; San Diego-Montgomery-Gibbs Executive Airport, CA (MYF); 13 February 2021
photo (c) Cedric Ma; San Diego-Montgomery-Gibbs Executive Airport, CA (MYF); 13 February 2021
photo (c) Noel Philips; San Diego-Montgomery-Gibbs Executive Airport, CA (MYF); 13 February 2021
photo (c) Noel Philips; San Diego-Montgomery-Gibbs Executive Airport, CA (MYF); 13 February 2021
Revision history:
Date/time | Contributor | Updates |