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ASN Wikibase Occurrence # 133235
Last updated: 21 November 2020
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Type:Silhouette image of generic P28A model; specific model in this crash may look slightly different
Piper PA-28-140
Owner/operator:Cherry Capital Aviation
Registration: N8255N
C/n / msn: 28-25466
Fatalities:Fatalities: 0 / Occupants: 4
Other fatalities:0
Aircraft damage: Written off (damaged beyond repair)
Location:Traverse, MI -   United States of America
Phase: Take off
Departure airport:
Destination airport:CVX
Investigating agency: NTSB
On July 19,1994, at 2016 eastern daylight time (edt), a Piper PA- 28-140, N8255N, registered to Cherry Capital Aviation of Traverse City, Michigan, and piloted by a private pilot, was destroyed when it collided with trees and terrain during a forced landing. The airplane had departed runway 18 at the Cherry Capital Airport shortly before the accident. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 flight was not operating on a flight plan. The pilot and two passengers received serious injuries, a third passenger received minor injuries. The flight departed Traverse City, Michigan, at 2013 edt.

N8255N's pilot was cleared for a left-hand turn out after takeoff from runway 18. At the time he was cleared, the controller was working a Cessna that was inbound for a left hand downwind to runway 18. After verifying the Cessna's position the controller changed N8255N's turnout direction to the right. N8255N's pilot acknowledged the clearance and turned to the right according to the controller.

One of N8255N's passenger's written statements said the airplane was climbing when the pilot was told to turn to the right. He said: "As we were turning, the plane bumped a little for approximately two to three seconds... ." He said after another passenger and he had made a comment about the "bumping" the airplane "...bumped again and again... ." Another passenger asked the pilot what the bumping was and the pilot said, according to the written statement, "Not good." The written statement continues, "As we were turning I noticed that we were slowly losing altitude... ." An interview with the passenger confirmed his written statement.

Witnesses observed the airplane fly past at a low altitude, repeatedly porpoising. The front seat passenger said the airplane began to "...wave..." back and forth soon after takeoff.

He said there were no engine problems during the flight. Two witnesses reported that N8255N's engine was running at "...full force..." and " climb power... ." One witness, a Michigan State Police Trooper, observed the airplane flying low and said it appeared to him that the airplane was too heavy for flight.

Before departing on the flight, the pilot of N8255N had it refueled with 34 gallons of fuel. The person refueling the airplane stated: "I thought it strange that four people were going in an aircraft with such a small useful load." The Grand Traverse Sheriff's Department obtained N8255N's occupants weights from their driver's licenses.

The passengers total weight was 685 pounds. The airplane's fuel weight was 204 pounds. Using the airplane's weight and balance data the airplane's takeoff gross weight and center of gravity were calculated. Its takeoff weight was 2,346 pounds and center of gravity (C.G.) was 90.6 aft of datum. N8255N's maximum gross weight was 2,150 pounds. Its C.G. range 88.6. to 96.0 inches aft of the datum at its maximum gross weight. The on-scene investigation revealed that airplane had full nose "UP" trim.

According to the pilot's logbook, his last flight in a Piper PA- 28-140 was July 1, 1992. His logbook showed one hour of dual instruction on that date. This flight was in N8255N. The remarks section stated: "Check-out/pleasure." There was no instructor signature in this entry. The next most current flight in the Piper PA-28 series airplane (PA-28-181) was on September 13, 1991, according to his logbook. During five months before the accident, the pilot had flown 4.9 hours in Cessna 150 airplanes.

N8255N's engine had a total time of 2,8821.7 hours on it before being overhauled. The engine had 118.7 hours since it was overhauled. The engine was sent to the manufacturer for test running. The test run was described as normal, the engine ran to the manufacturer's specifications. The runup test report is appended to this report.

The NTSB Form 6120.1/2 was not filed by the pilot due to his injuries.
PROBABLE CAUSE:poor preflight planning and preparation by


NTSB id 20001206X01702

Revision history:

21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]

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