ASN Wikibase Occurrence # 133768
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Date: | Thursday 18 December 1997 |
Time: | 21:20 LT |
Type: | Piper PA-28R-200 |
Owner/operator: | Congressional Air Charter Inc |
Registration: | N9418N |
MSN: | 28R-35130 |
Year of manufacture: | 1969 |
Total airframe hrs: | 3852 hours |
Engine model: | Lycoming IO-360 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Skidmore, WV -
United States of America
|
Phase: | En route |
Nature: | Executive |
Departure airport: | Charleston, WV (CRW |
Destination airport: | Gaithersburg, MD (GAI |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was in cruise flight at 7,500 feet with the engine producing satisfactory power. The pilot said the engine slowly and smoothly lost power over a 10-15 second duration. The engine completely lost power over an unlighted rural area and the pilot struck trees and collided with terrain during the subsequent forced landing. Examination of aircraft records revealed the engine and the fuel control were overhauled by their respective manufacturers and the engine was installed 2 weeks prior to the accident. The engine had accumulated 14.6 hours since overhaul. Examination of the engine revealed no mechanical deficiencies. Examination of the fuel control servo revealed that a lock nut was no longer installed. The initial flow tests revealed a flow rate equivalent to idle cut off. When a test nut was installed, the unit flowed 'perfectly.' When questioned about the performance of the fuel servo and the engine with the outer nut no longer installed in the servo, the Inspector stated, 'Basically, what it does is it shuts off the fuel when that nut backs off. It's just like pulling it to idle cut off.'
Probable Cause: an improper overhaul of the fuel servo by the manufacturer, which resulted in the loss of engine power. Factors in the accident were the dark night conditions and rough forced landing terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC98LA045 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB NYC98LA045
Location
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
08-Apr-2024 11:28 |
ASN Update Bot |
Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report] |
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