Accident Piper PA-28R-200 N9418N,
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ASN Wikibase Occurrence # 133768
 
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Date:Thursday 18 December 1997
Time:21:20 LT
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-200
Owner/operator:Congressional Air Charter Inc
Registration: N9418N
MSN: 28R-35130
Year of manufacture:1969
Total airframe hrs:3852 hours
Engine model:Lycoming IO-360
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Skidmore, WV -   United States of America
Phase: En route
Nature:Executive
Departure airport:Charleston, WV (CRW
Destination airport:Gaithersburg, MD (GAI
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was in cruise flight at 7,500 feet with the engine producing satisfactory power. The pilot said the engine slowly and smoothly lost power over a 10-15 second duration. The engine completely lost power over an unlighted rural area and the pilot struck trees and collided with terrain during the subsequent forced landing. Examination of aircraft records revealed the engine and the fuel control were overhauled by their respective manufacturers and the engine was installed 2 weeks prior to the accident. The engine had accumulated 14.6 hours since overhaul. Examination of the engine revealed no mechanical deficiencies. Examination of the fuel control servo revealed that a lock nut was no longer installed. The initial flow tests revealed a flow rate equivalent to idle cut off. When a test nut was installed, the unit flowed 'perfectly.' When questioned about the performance of the fuel servo and the engine with the outer nut no longer installed in the servo, the Inspector stated, 'Basically, what it does is it shuts off the fuel when that nut backs off. It's just like pulling it to idle cut off.'

Probable Cause: an improper overhaul of the fuel servo by the manufacturer, which resulted in the loss of engine power. Factors in the accident were the dark night conditions and rough forced landing terrain.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC98LA045
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB NYC98LA045

Location

Revision history:

Date/timeContributorUpdates
21-Dec-2016 19:26 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
08-Apr-2024 11:28 ASN Update Bot Updated [Time, Other fatalities, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

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