ASN Wikibase Occurrence # 134089
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Date: | Friday 30 August 1996 |
Time: | 14:30 |
Type: | Piper PA-22-108 |
Owner/operator: | Houck, Stanley E. |
Registration: | N4992Z |
MSN: | 22-8600 |
Year of manufacture: | 1961 |
Total airframe hrs: | 2800 hours |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Ashland, OR -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | S03 |
Destination airport: | 77S |
Investigating agency: | NTSB |
Confidence Rating: | Information is only available from news, social media or unofficial sources |
Narrative:On August 30, 1996, about 1430 Pacific daylight time, N4992Z, a Piper PA-22, operated by the owner/pilot, had an in-flight fire and was destroyed after an emergency landing at Ashland, Oregon. The in-flight fire was first detected during the initial climbout from Ashland. The private pilot and his passenger were not injured. Visual meteorological conditions prevailed and no flight plan had been filed. The personal flight was conducted under 14 CFR 91 and was destined for Creswell, Oregon.
According to the pilot in a telephone interview on the day of the accident, the airplane underwent a "good" preflight and engine run-up prior to departure from runway 30 at the Ashland Municipal Airport. The pilot stated that no anomalies were detected prior to the takeoff, and that the ammeter was showing about "a 1/2 needle-width of charge." During the initial climbout, the pilot smelled something burning. Shortly thereafter, at an altitude of about 250 feet above the ground, the pilot saw white smoke coming from underneath the left portion of the instrument panel. The pilot stated that he checked the circuit breakers, and none had popped. He shut off the airplane's electrical equipment and commenced an immediate turn back to the departure airport.
The pilot further stated in a written statement (attached) that he entered the traffic pattern for landing on runway 30. He turned the electrical master switch back on to announce his intentions of the radio, and then turned the switch off. The smoke turned black and began to get thicker; he then observed a small flame coming from underneath the instrument panel. The engine quit just short of the runway. While on final approach and during the flare over the runway, the pilot could not see outside of the airplane. He felt the airplane touch down. He attempted to activate the brake, and it was ineffective. The airplane veered off the left side of the runway and into grass. As it slowed, the pilot got his passenger to exit the airplane, followed by himself. The airplane came to a stop and burned. It was completely consumed in the fire, except for the engine and a portion of the right wing.
According to the Oregon State Fire Marshall fire investigation report (attached):
... the exhaust pipe connecting to the muffler was not connected. It had come apart a distance of approximately 1-1/2". Back towards the engine where the exhaust pipe entered the manifold portion of the exhaust system I noted a new crack approximately half way around the pipe. My determination that the crack was new was due to the [shiny] appearance of the metal in the crack area. The spread of the crack was in direct relation to the distance the pipe was pulled out of the muffler. My opinion finds that the heat from the exhaust pipe disconnection was in close proximity to the voltage regulator on the firewall above the connection point. It was apparent ... that the heat melted the insulation on the wiring short circuiting the wiring in all directions leading to and from the voltage regulator. The resulting short circuit began to smoke....increased oxygen [due to opening of the cabin doors after landing] intensified the ignition and brought it into full flame.
According to an FAA aviation safety inspector (statement attached) from Portland, Oregon:
... the left exhaust pipe was cracked at the rear riser and separated from the muffler. The exhaust pipe muffler clamp was loose and worn. The clamp has a knob welded to the interior side. This knob extends through the exhaust pipe and muffler inlet to prevent the separation of the two. The clamp bolts to the pipe. The knob on the clamp appeared to be badly worn and the insertion holes in the pipe and muffler were elongated.
The FAA inspector further stated that FAA Airworth
Sources:
NTSB id 20001208X06641
Revision history:
Date/time | Contributor | Updates |
21-Dec-2016 19:26 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
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