ASN Wikibase Occurrence # 145409
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Date: | Wednesday 2 May 2012 |
Time: | 07:15 |
Type: | Glasair I |
Owner/operator: | Private |
Registration: | N540GZ |
MSN: | 208 |
Total airframe hrs: | 84 hours |
Engine model: | Lycoming O-540-E4B5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Columbus Metropolitan Airport - KCSG, Columbus, GA -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | Columbus, GA (CSG) |
Destination airport: | Montgomery, AL (MGM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was attempting to take off in an experimental tailwheel-equipped airplane. He stated that the airplane started to accelerate forward on the takeoff roll and pull to the left while he had right rudder applied. The engine hesitated, and he applied more right rudder and full right brake with no results. He aborted the takeoff and applied both brakes to slow the airplane. The airplane exited the left side of the runway and collided with a runway sign; the left main landing gear collapsed, which resulted in structural damage to the airframe. The pilot reported that he had 0.1 hour in the accident airplane make and model. Examination of the wreckage, including the brakes, did not reveal any preimpact mechanical malfunctions or failures that would have precluded normal operation. The engine was subsequently test run at full throttle and no anomalies were noted. The airplane owner’s manual indicated that for takeoff, the flaps should be set at 20 degrees and that power should be added slowly to allow airspeed to build and the controls to become effective by the time full power is achieved. Examination of the wreckage revealed that the flaps were in the retracted position. The pilot’s lack of experience in the airplane make and model and unfamiliarity with its operating procedures contributed to his failure to use the recommended flap setting for takeoff.
Probable Cause: The pilot’s failure to maintain directional control during takeoff, which resulted in a runway excursion and collision with a runway sign. Contributing to the accident was the pilot’s lack of experience in the airplane make and model, resulting in and his failure to use the recommended flap setting for takeoff.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA12LA315 |
Status: | Investigation completed |
Duration: | 1 year and 4 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
03-May-2012 17:50 |
Geno |
Added |
03-May-2012 23:51 |
Geno |
Updated [Time, Aircraft type, Nature, Destination airport, Source, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
27-Nov-2017 20:42 |
ASN Update Bot |
Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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