Accident Hughes OH-6A N368PD,
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ASN Wikibase Occurrence # 150511
 
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Date:Saturday 3 November 2012
Time:22:45
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes OH-6A
Owner/operator:Atlanta City Police
Registration: N368PD
MSN: 1180900
Year of manufacture:1967
Total airframe hrs:6528 hours
Engine model:Rolls-Royce T63-A720
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:NW Atlanta, GA -   United States of America
Phase: Manoeuvring (airshow, firefighting, ag.ops.)
Nature:Unknown
Departure airport:Atlanta Hartsfield-Jackson International Airport, GA (ATL/KATL)
Destination airport:Atlanta Hartsfield-Jackson International Airport, GA (ATL/KATL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The night, public flight was being operated to support ground-based police personnel in locating a missing child. Witnesses reported observing the helicopter at a very low altitude with the search light on maneuvering near the intersection of two city streets. Witness statements indicated that, as the helicopter neared the intersection, the landing gear skids collided with wires at the top a 42-foot power pole. The helicopter then flipped over and crashed into the street. Recorded radar data were consistent with the witness statements. An examination of the airframe did not reveal evidence of malfunctions or failures that would have precluded normal operation. Rotational scoring found on the internal engine components indicates that the engine had power at impact. No distress calls were received from the flight crew before the crash. Most of the pilot’s peers described him as “meticulous,” “capable,” and “competent”; however, one pilot stated that the accident pilot had a tendency to “fly low.”
Probable Cause: The pilot's failure to maintain sufficient altitude during maneuvering flight, which resulted in his failure to see and avoid a power pole and wires.
N368PD deregistered Jul 2014. Ex US Army 67-16515.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA13GA046
Status: Investigation completed
Duration: 1 year and 4 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=368PD&x=0&y=0

Location

Revision history:

Date/timeContributorUpdates
04-Nov-2012 01:24 gerard57 Added
04-Nov-2012 01:25 gerard57 Updated [Aircraft type]
04-Nov-2012 06:40 monuerunt Updated [Narrative]
04-Nov-2012 09:48 Black Typhoon Updated [Time, Aircraft type]
05-Nov-2012 11:20 Geno Updated [Aircraft type, Registration, Cn, Location, Phase, Nature, Source, Narrative]
21-Dec-2016 19:28 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
28-Nov-2017 13:54 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]
02-Jul-2022 09:20 rvargast17 Updated [Source, Damage, Narrative]
31-May-2023 05:17 Ron Averes Updated [[Source, Damage, Narrative]]

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