ASN Wikibase Occurrence # 150748
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Date: | Sunday 11 November 2012 |
Time: | 15:30 |
Type: | Tecnam P2004 Bravo |
Owner/operator: | Plus One Flyers |
Registration: | N153TB |
MSN: | 081 |
Total airframe hrs: | 1104 hours |
Engine model: | Rotax 912ULS |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | McClellan-Palomar Airport (KCRQ), Carlsbad, California -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Carlsbad, CA (CRQ) |
Destination airport: | Carlsbad, CA (CRQ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot intended to practice touch-and-go landings on a runway nearly aligned with the reported 9-knot wind, in clear weather conditions. He noted no mention of any wind gusts in the airport’s automatic terminal information service weather information before he took off. However, the pilot noticed light turbulence during the right crosswind and downwind legs in the traffic pattern. After a short approach and a smooth landing, he applied power, achieved rotation speed, and lifted off again. However, when the airplane was only a few feet off the ground, the wind started to blow it left of the center line. Although the pilot applied full rudder and aileron deflection to counter the crosswind, the airplane continued to track toward the side of the runway and was not climbing at a rate that would clear parked aircraft. The pilot aborted the takeoff, and the airplane subsequently collided with the tail of a parked helicopter, spun a few degrees clockwise, and came to rest on its left wing, which sustained substantial damage. The pilot reported no preimpact mechanical malfunctions or failures with the airplane that would have precluded normal operation.
The pilot reported that he had flown about 3 hours in the accident airplane, which was a light sport airplane. He believed that because of the airplane’s relatively light weight, it was more susceptible to crosswind and turbulence than other airplanes he had flown. He also noted that the controls were configured significantly different than any of the other airplanes he had flown. His previous flights took place in calm air, and the pilot thought that his time in the accident airplane was insufficient to instill the reflexive familiarity necessary to control the airplane during the accident takeoff.
Probable Cause: The pilot’s failure to maintain directional control during takeoff, which resulted in a runway excursion and collision with parked aircraft. Contributing to the accident was the pilot's lack of experience in the airplane make/model.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR13CA039 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
18-Nov-2012 11:26 |
Goldfish85 |
Added |
18-Nov-2012 11:28 |
harro |
Updated [Aircraft type, Registration, Operator, Total fatalities, Other fatalities, Source, Damage] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
28-Nov-2017 13:54 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
30-Jun-2018 11:19 |
SANMJN |
Updated [Other fatalities, Location] |
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