ASN Wikibase Occurrence # 161717
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Date: | Sunday 27 October 2013 |
Time: | 17:40 |
Type: | Bellanca 14-19-3 Cruisemaster |
Owner/operator: | Private |
Registration: | N11RC |
MSN: | 4279 |
Year of manufacture: | 1966 |
Total airframe hrs: | 2812 hours |
Engine model: | Continental IO-470-F1 |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | near Boerne, TX -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Fulton Airport, MO (FTT) |
Destination airport: | San Antonio Airport, TX (8T8) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was returning to his home airport. A review of radar data showed the accident airplane in a straight-line descent from cruise flight at a rate of nearly 2,900 ft per minute. The descent resulted in a loss of 8,100 ft in less than 3 minutes until the airplane disappeared from radar in the vicinity of the accident site.
Disassembly of the airplane’s cabin heat shroud, which provided heated air to the cabin, revealed evidence of cracks and holes in the muffler wall and exhaust gas penetration into the interior of the shroud. According to the autopsy report, the pilot died as a result of thermal injuries and smoke inhalation, with soot present in the upper airway and 37% carbon monoxide found in his blood postmortem. Based on the lack of soot in the lower airway and the elevated carbon monoxide levels, the majority of the carbon monoxide in the pilot’s blood was likely from inhalation during the flight at levels that would have impaired his ability to safely fly the airplane. Although cetirizine, also known as Zyrtec® (used to temporarily relieve allergy symptoms and could cause drowsiness), was also detected in the pilot’s urine and blood, the detected level indicated that impairment from the drug was unlikely.
Probable Cause: A defective exhaust system that allowed carbon monoxide to enter the cabin and impair the pilot, rendering him unable to control the airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN14FA024 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=11RC
History of this aircraft
Other occurrences involving this aircraft
2 August 1999 |
N8509R |
Private |
0 |
North Platte, NE |
|
sub |
Fuel exhaustion |
Location
Images:
Photo: NTSB
Revision history:
Date/time | Contributor | Updates |
28-Oct-2013 02:06 |
Geno |
Added |
28-Oct-2013 02:20 |
Geno |
Updated [Time, Total fatalities, Other fatalities, Source, Narrative] |
28-Oct-2013 16:35 |
Geno |
Updated [Aircraft type, Registration, Cn, Operator, Total occupants, Source, Damage, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
29-Nov-2017 09:19 |
ASN Update Bot |
Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative] |
20-May-2022 18:59 |
Captain Adam |
Updated [Other fatalities, Location, Phase, Departure airport, Destination airport, Source, Narrative, Category, Photo] |
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