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ASN Wikibase Occurrence # 165209
Last updated: 19 August 2019
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Date:23-JUL-2013
Time:06:31 UTC
Type:Silhouette image of generic B734 model; specific model in this crash may look slightly different
Boeing 737-405
Owner/operator:SAS Scandinavian Airlines
Registration: LN-BRE
C/n / msn: 24643/1860
Fatalities:Fatalities: 0 / Occupants:
Other fatalities:0
Aircraft damage: Minor
Location:København-Kastrup Airport (CPH/EKCH) -   Denmark
Phase: Take off
Nature:International Scheduled Passenger
Departure airport:København-Kastrup Airport (CPH/EKCH)
Destination airport:Oslo-Gardermoen Airport (GEN/ENGM)
Narrative:
A SAS Boeing 737-400 operated on scheduled flight, SK-1462, from Copenhagen, Denmark to Oslo/Gardermoen in Norway.
Following initial take-off from runway 04R at Copenhagen, the flight crew noticed a flock of birds in front of the aircraft. Immediately thereafter – at approximately 800 feet AGL – a "bang" was heard in the aircraft and the flight crew noticed a smell of burned material from the air conditioning system.
One or more birds hit the left engine which resulted in abnormal engine vibrations.
The flight crew advised the aerodrome control tower of the bird strike and requested a return for landing.
Since the left engine developed power and except for the vibration level there was no abnormal engine indications, the captain decided to return and perform the final approach and landing with
both engines running.
The aircraft landed safely on runway 04R. The airport fire and rescue services followed the aircraft and observed fluid leaking from the bottom of the left engine. Therefore, the Tower controller instructed the flight crew to taxi to a deicing platform were the the crew and passengers disembarked the aircraft.

AIB Denmark noted that the number of bird strikes at Copenhagen had decreased from 141 in 2012 to 105 in 2013 and did not issue any safety recommendations.

The serious incident was caused by a birdstrike to the left engine.
One or more Common Shelducks damaged the left air intake duct and the engine fan which resulted in abnormal vibrations and a fuel leak from the left engine.

A contributing factor to the serious incident was:
As a result of the altitude AGL of the birds, it was not possible for EKCH’s Wildlife Control Unit to observe and act against the flock of migrating Common Shelducks.

Sources:

http://havarikommissionen.dk/~/media/Files/Havarikommissionen/Havarirapporter/Luftfart%202013/HCLJ510_2013_234%20_%20Bulletin.ashx


Images:

Photo of LN-BRE courtesy AirHistory.net


Barcelona (LEBL / BCN)
13 July 2003; (c) Toni Marimón

Revision history:

Date/timeContributorUpdates
03-Apr-2014 20:16 harro Added
03-Apr-2014 20:19 harro Updated [Narrative]

Corrections or additions? ... Edit this accident description