ASN Wikibase Occurrence # 167952
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 22 June 2014 |
Time: | 17:40 LT |
Type: | Stampe SV.4C |
Owner/operator: | Private |
Registration: | G-BPLM |
MSN: | 1004 |
Year of manufacture: | 1948 |
Engine model: | De Havilland Gipsy Major 10 MK.2 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | ½ nm north-west of Paddock Wood, Tunbridge Wells, Kent, England -
United Kingdom
|
Phase: | En route |
Nature: | Private |
Departure airport: | Clutton Hill, Somerset |
Destination airport: | Maidstone-Lashenden (Headcorn) Airfield (EGKH) |
Investigating agency: | AAIB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On passing Redhill, during a flight from Clutton Hill in Somerset to Headcorn in Kent, the pilot checked he had sufficient fuel for the remaining 25 nm of the flight. Just west of Paddock Wood, at 1,700 ft amsl, the aircraft was caught in a “particularly harsh” thermal, shortly after which the engine “coughed”.
The pilot considered this to be so unusual that he decided to land immediately at Old Hay Airfield, 1 nm east of Paddock Wood; however, the engine then stopped. He checked the mixture, fuel and magnetos and set up for a forced landing in what looked like a hay field. At about 100 ft, positioned to land a third of the way into the field, the pilot realized the crop was rapeseed which he knew was much denser than hay.
To try to reduce his forward speed on touchdown, he “deep stalled” the aircraft just above the crop; however, the undercarriage caught in the rapeseed and the aircraft slowly pitched over onto its back. With the magnetos and fuel off, he released his full harness and additional lap strap before vacating the aircraft unhurt. The pilot suspected that the problem was caused by the carburettor’s float needle jamming in its base – a problem he was aware had occurred on another Stampe at Headcorn in 2013.
Accident investigation:
|
| |
Investigating agency: | AAIB |
Report number: | EW/G2014/06/38 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
1. AAIB:
https://assets.digital.cabinet-office.gov.uk/media/548b1252ed915d4c0d0002ae/Stampe_SV4C__Modified__Stampe_G-BPLM_12-14.pdf 2. CAA:
http://www.caa.co.uk/aircraft-registration/ 3.
http://www.bea.aero/fr/enquetes/2014/2014.semaine.28.pdf Revision history:
Date/time | Contributor | Updates |
17-Jul-2014 09:21 |
harro |
Added |
30-Jul-2014 11:38 |
Alpine Flight |
Updated [Time, Aircraft type] |
13-Dec-2014 10:24 |
Dr. John Smith |
Updated [Registration, Cn, Operator, Location, Phase, Nature, Departure airport, Destination airport, Source, Embed code, Narrative] |
30-Sep-2015 20:34 |
Dr. John Smith |
Updated [Destination airport, Source, Embed code] |
29-Jun-2020 05:15 |
harro |
Updated [Destination airport, Accident report, ] |
26-Jun-2023 09:24 |
Nepa |
Updated [[Destination airport, Accident report, ]] |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation