ASN Wikibase Occurrence # 168243
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Date: | Thursday 17 July 2014 |
Time: | 15:15 |
Type: | Piper PA-30 Twin Comanche |
Owner/operator: | Private |
Registration: | N7981Y |
MSN: | 30-1082 |
Year of manufacture: | 1966 |
Engine model: | Lycoming IO-320 SERIES |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Othello Municipal Airport, Othello, Washington -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | Othello, WA (S70) |
Destination airport: | Klamath Falls, OR (KLMT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot of the twin-engine airplane was preparing to take off for a cross-country flight. He reported that during the power up for takeoff, the left engine was at 2,200 rpm while the right engine was at 2,600 rpm. He leaned the mixture on the left engine to bring the rpm up to 2,600 and proceeded with the takeoff. After the takeoff roll, he started to climb the airplane and noted that the exhaust gas temperature on the left engine was much higher than on the right engine. The left engine rpm suddenly dropped to 2,000, and the airplane yawed to the left and started to descend. The pilot could not stop the yaw and descent, and the airplane impacted the ground, which resulted in substantial damage.
The pilot reported that he should not have leaned the left engine for takeoff.
A review of the left engine's logbook revealed a logbook entry about 4 months before the accident noting that the fuel flow divider, fuel servo, and turbo charger had been removed, repaired, and reinstalled. The entry also noted that a flow test was performed and that the engine was tested, checked for leaks, and returned to service.
The airplane and engines were sold for salvage and were not available for examination; therefore, the reason for the partial loss of engine power could not be determined.
Probable Cause: The partial loss of engine power for reasons that could not be determined based on the available information.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR14LA298 |
Status: | Investigation completed |
Duration: | 5 years and 9 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register: 2. FAA:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?omni=Home-N-Number&nNumberTxt=7981Y 3.
https://flightaware.com/resources/registration/N7981Y Location
Revision history:
Date/time | Contributor | Updates |
03-Aug-2014 20:15 |
Geno |
Added |
28-Feb-2016 20:35 |
Dr.John Smith |
Updated [Time, Departure airport, Destination airport, Source, Narrative] |
21-Dec-2016 19:28 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
17-Apr-2017 22:08 |
Dr.John Smith |
Updated [Time, Location, Destination airport, Damage, Narrative] |
19-Apr-2020 07:03 |
ASN Update Bot |
Updated [Time, Operator, Departure airport, Destination airport, Source, Damage, Narrative, Accident report, ] |
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