Accident Piper PA-28R-200 N33840,
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ASN Wikibase Occurrence # 177627
 
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Date:Sunday 16 May 2004
Time:14:15
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-200
Owner/operator:Private
Registration: N33840
MSN: 28R-7535205
Year of manufacture:1975
Total airframe hrs:5481 hours
Engine model:Lycoming IO-360-C1C
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Everglades City, FL -   United States of America
Phase: Take off
Nature:Private
Departure airport:Everglades City, FL (X01)
Destination airport:Tampa, FL (TPF)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that he performed a run-up of the engine prior to departing the airport and found no problems. He said he then back-taxied to runway 15 for departure and during the take-off roll, the engine seemed to be fine. He further stated that at 65-68 knots he rotated but the aircraft did not leave the ground so he let the aircraft accelerate to 75 knots. The pilot says he then pulled back on the yoke, and the aircraft lifted off the runway and torqued to the left which he attempted to counteract by using the right rudder. He said that at this point the engine seemed "diminished" but that it was not sputtering. He said he then lowered the nose and the aircraft began descending at which time he lowered the landing gear. He says he saw a small island of trees and set the aircraft down in the trees. The passenger seated in the right front seat stated that before takeoff the pilot performed an engine check and it was running fine. During the takeoff roll the pilot pulled the aircraft up at about 65 miles per hour. He thought they were lifting off early for they still had over half of the runway left. The pilot pulled the nose up too steep and at about 300 feet the airplane began to stall and the left wing dropped. The pilot tried to gain speed by dropping the nose and leveling off. They did not have enough altitude and the airplane kept dropping and went into the trees. As far as he could tell there was nothing wrong with the airplane. Postcrash examination and testing of the airplane structure and flight control systems, airplane and engine fuel system, engine, propeller, fuel control, propeller governor, and the stall warning system switch showed no evidence of precrash failure or malfunction.
Probable Cause: The failure of the pilot to maintain airspeed during climb after takeoff resulting in an inadvertent stall, uncontrolled descent, and impact in a wooded area.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA04LA084
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040520X00620&key=1

Location

Revision history:

Date/timeContributorUpdates
07-Jul-2015 14:54 Noro Added
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
07-Dec-2017 17:59 ASN Update Bot Updated [Other fatalities, Departure airport, Destination airport, Source, Narrative]

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