ASN Wikibase Occurrence # 177918
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Date: | 31-MAY-2004 |
Time: | 12:15 |
Type: | Rockwell S-2R Thrush Commander |
Owner/operator: | Private |
Registration: | N5686X |
MSN: | 2359R |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Other fatalities: | 0 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Beaver, UT -
United States of America
|
Phase: | Landing |
Nature: | Agricultural |
Departure airport: | Beaver, UT (U52) |
Destination airport: | Beaver, UT (U52) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, he had finished spraying a field and was returning to the airport for another load. He said that he had half a tank of fuel remaining and the engine was producing "excellent power." A few moments later, the engine ran rough for about a second and then stopped. He did not notice anything coming out of the exhaust. The pilot tried twice to restart the engine but was unsuccessful and he attempted a forced landing to an open field. During the landing, the airplane impacted terrain and struck a fence. Both wings were displaced aft and the right main landing gear was collapsed. A visual examination of the engine revealed a 360 degree crack around the P3 air pressure tube, causing a separation of the tube between the engine plenum and fuel control unit. The crack was approximately one-quarter inch aft of the "B" nut, which connects the P3 air pressure tube to the fuel control unit. There was a "notable" amount of carbon build-up in the area around the crack. According to a maintenance representative, failure of the tube in flight would have resulted in a "significant reduction in fuel scheduling which could result in an engine flameout." An attempt to restart the engine in flight would "likely have failed," however; an attempt would have accounted for the "notable" amount of carbon build-up around the break in the tube. No other aircraft anomalies were noted.
Probable Cause: the in-flight failure of the engine's P3 tube which resulted in the loss of engine power and the subsequent impact with terrain during a forced landing. Contributing factors include the lack of suitable terrain for a forced landing and the fence.
Sources:
NTSB:
https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20040615X00792&key=1
Revision history:
Date/time | Contributor | Updates |
18-Jul-2015 16:31 |
Noro |
Added |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Dec-2017 17:58 |
ASN Update Bot |
Updated [Cn, Other fatalities, Departure airport, Destination airport, Source, Narrative] |
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