Accident Cessna TU206G Turbo Stationair N235HM,
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ASN Wikibase Occurrence # 178270
 
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Date:Monday 3 August 2015
Time:10:00
Type:Cessna TU206G Turbo Stationair
Owner/operator:Private
Registration: N235HM
MSN: U20606795
Year of manufacture:1984
Total airframe hrs:2316 hours
Engine model:Continental TSIO520M
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:St. Ignatius, Lake County, MT -   United States of America
Phase: Landing
Nature:Private
Departure airport:Bozeman, MT (B2N)
Destination airport:Polson, MT (8S1)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was conducting the airplane’s first flight since the engine had undergone maintenance several months earlier. He reported that, after about 45 minutes of flight, he noticed that the exhaust gas temperature (EGT) had increased but that he was able to reduce the temperature by increasing the fuel flow. Shortly after, the EGT again increased, and the pilot began to troubleshoot the issue. The pilot stated that, after he turned the electric fuel boost pump on a second time, the engine ran normally for about 2 minutes and then lost power. He determined that the airplane would be unable to reach the airport, so he initiated a forced landing to a road. During the landing roll, the airplane struck vegetation and a fence.
During a postaccident examination of the airplane, blue fuel stains were observed on the top of the engine. The fuel line attached to the fuel flow transducer was found finger tight and leaking. A review of the airplane’s maintenance records indicated that, during the maintenance conducted several months before the accident, three cylinders, including the No. 6 cylinder, had been removed and reinstalled. The fuel line attached to the fuel flow transducer was just above the No. 6 cylinder and, therefore, it would been removed to access the cylinder during the maintenance. It is likely that maintenance personnel did not adequately tighten the fuel line during its reinstallation, which led to the loss of fuel pressure and the subsequent loss of engine power.

Probable Cause: Maintenance personnel’s failure to tighten a fuel line, which resulted in a loss of fuel pressure and a subsequent loss of engine power during cruise flight and an off-airport landing and collision with obstacles.

Accident investigation:
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Investigating agency: NTSB
Report number: WPR15LA229
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=235HM

Location

Revision history:

Date/timeContributorUpdates
04-Aug-2015 05:06 Geno Added
04-Aug-2015 16:36 Geno Updated [Aircraft type, Registration, Cn, Operator, Nature, Source]
21-Dec-2016 19:30 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
01-Dec-2017 15:07 ASN Update Bot Updated [Operator, Other fatalities, Departure airport, Destination airport, Source, Narrative]

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