ASN Wikibase Occurrence # 180296
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Date: | Saturday 10 October 2015 |
Time: | 14:00 |
Type: | Cessna 172S Skyhawk |
Owner/operator: | Private |
Registration: | N5295Y |
MSN: | 172S9236 |
Year of manufacture: | 2002 |
Total airframe hrs: | 6119 hours |
Engine model: | Lycoming IO-360-L2A |
Fatalities: | Fatalities: 1 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Volusia County north of Seville, FL -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Private |
Departure airport: | Daytona, FL (DAB) |
Destination airport: | Daytona, FL (DAB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot reported that, during a local flight, he encountered a downdraft while maneuvering the airplane between 300 and 600 ft above ground level at an airspeed about 75 knots. He stated that he attempted to recover, but the airplane continued to sink and subsequently impacted trees and terrain. Postaccident examination of the airplane did not reveal evidence of any mechanical any anomalies that would have precluded normal operation.
The conditions reported by the closest weather observation facility, located 23 nautical miles away, included scattered towering cumulus clouds and 6-knot winds. Additionally, towering cumulus and cumulonimbus clouds were noted near the airport. Atmospheric modeling data noted the potential for strong low-level thermal activity near the accident site about the time of the accident. Given the weather conditions that prevailed about the time of the accident, it is likely that the airplane encountered a downdraft; given the airplane's altitude and airspeed at the time of the encounter, the pilot had insufficient time to regain control of the airplane before it impacted the ground.
Probable Cause: The airplane’s encounter with a downdraft, and the pilot's decision to maneuver the airplane at a low altitude and airspeed, which provided insufficient time and altitude to recover before impacting terrain.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA16LA008 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
10-Oct-2015 23:42 |
Geno |
Added |
13-Oct-2015 22:06 |
Geno |
Updated [Source, Damage, Narrative] |
21-Dec-2016 19:30 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
07-Feb-2018 13:48 |
ASN Update Bot |
Updated [Time, Operator, Nature, Departure airport, Destination airport, Source, Narrative] |
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