Accident Montgomerie-Bensen B8M G-BPFK,
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ASN Wikibase Occurrence # 187780
 
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Date:Sunday 6 November 1994
Time:
Type:Silhouette image of generic b8 model; specific model in this crash may look slightly different    
Montgomerie-Bensen B8M
Owner/operator:Private
Registration: G-BPFK
MSN: PFA G/01A-1116
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Destroyed
Category:Accident
Location:Enstone Airfield, 4.5nm East of Chipping Norton, Oxfordshire -   United Kingdom
Phase: Approach
Nature:Training
Departure airport:Enstone Airfield, Oxfordshire (EGTN)
Destination airport:Enstone Airfield, Oxfordshire (EGTN)
Investigating agency: AAIB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Written off (destroyed) 6-11-1994 when crashed at Enstone Airfield, 4.5 nautical miles East of Chipping Norton, Oxfordshire. The pilot (the sole person on board) survived, but was seriously injured. According to the following extract from the official AAIB report into the accident:

"When the accident pilot arrived at Enstone, he was offered G-BPFK to fly. Following an initial taxi run to 'get the feel of the aircraft' (although he had flown it once before) he took off and carried out a tight right hand circuit at approximately 200 feet agl.

After he completed his final turn, the aircraft was seen to dive, and the engine power was heard to increase; G-BPFK then flew along the length of the runway at low level and high speed. At the end of the runway, the autogyro then went into a steep climb to approximately 250 feet agl.

With the airspeed at near zero at the top of the climb, G-BPFK turned sharply through 180 degrees, and then entered a dive; everything appeared to be normal although there was no apparent reduction in engine power. After a loss of approximately 150 feet in altitude, the angle of the dive was seen to increase dramatically, and the autogyro impacted the ground almost vertically, in a nose down position.

The pilot was recovered from the autogyro unconscious, and his crash helmet had come off in the crash. Fortunately, there was a doctor present at the airfield, and she was on the scene within minutes. Subsequently, following his release from hospital, the pilot could not remember anything about the accident flight."

Damage sustained to airframe: Per the AAIB report "aircraft destroyed". However, the registration G-BPFK was only cancelled by the CAA on 20-10-2000, almost six year later.

Accident investigation:
cover
  
Investigating agency: AAIB
Report number: 
Status: Investigation completed
Duration:
Download report: Final report

Sources:

1. AAIB: https://assets.digital.cabinet-office.gov.uk/media/5422fedee5274a13170009f3/Montgomerie-Bensen_B8MR_Autogyro__G-BPFK_04-95.pdf
2. CAA: https://siteapps.caa.co.uk/g-info/rk=BPFK

Revision history:

Date/timeContributorUpdates
01-Jun-2016 16:33 Dr.John Smith Added

Corrections or additions? ... Edit this accident description

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