ASN Wikibase Occurrence # 188990
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Date: | Monday 1 August 2016 |
Time: | 11:00 |
Type: | Lancair 360 |
Owner/operator: | Private |
Registration: | N528HZ |
MSN: | 553-320-300 |
Year of manufacture: | 2014 |
Engine model: | Lycoming IO-360-C1C |
Fatalities: | Fatalities: 1 / Occupants: 1 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Columbia Gorge Regional (KDLS), Dallesport, OR -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | The Dalles, OR (DLS) |
Destination airport: | The Dalles, OR (DLS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was landing the airplane on runway 31 in visual meteorological conditions when witnesses observed the airplane in a nose-low, steep-left-bank attitude west of the runway over grassy terrain. A second later, the airplane impacted the terrain. An examination of the accident site revealed propeller slash marks about 1,800 ft from the approach end of runway 31. The initial point of a 200-foot-long debris path was located 385 ft from the slash marks on a 235° magnetic heading, and the airplane came to rest upright at the end of the debris path with its nose oriented northeast.
During the wreckage recovery, both main and the nose landing gear were found in a retracted position. During the postaccident examination, the throttle, mixture and propeller control levers were observed positioned full forward. The left and right main landing gear doors and the fuselage bottom skin exhibited numerous scratches and paint transfer consistent with the airplane's lower surface contacting the runway with the landing gear retracted. Both propeller blade tips were bent and curled aft, and the blades displayed numerous span-wise scratches from about mid span to the blade tips consistent with the propeller blades contacting the runway. The examination revealed no evidence of any preimpact mechanical failures or anomalies that would have precluded normal operation.
It is likely that, during the landing sequence, the pilot realized that the landing gear was retracted and aborted the landing by adding full power. During the aborted landing, the pilot did not maintain control of the airplane, which rolled to the left and impacted terrain.
Probable Cause: The pilot's loss of control during an aborted landing. Contributing to the accident was the pilot's failure to extend the landing gear before touchdown.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR16FA154 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=528HZ Location
Revision history:
Date/time | Contributor | Updates |
01-Aug-2016 22:37 |
Geno |
Added |
01-Aug-2016 22:46 |
Geno |
Updated [Phase, Destination airport, Source, Narrative] |
02-Aug-2016 15:33 |
Rob |
Updated [Registration, Operator, Total fatalities, Source] |
02-Aug-2016 15:34 |
harro |
Updated [Aircraft type, Operator] |
02-Aug-2016 17:01 |
Iceman 29 |
Updated [Cn, Source] |
15-Jan-2018 20:38 |
ASN Update Bot |
Updated [Time, Cn, Nature, Departure airport, Destination airport, Source, Narrative] |
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