ASN Wikibase Occurrence # 191041
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Date: | Saturday 29 October 2016 |
Time: | 15:40 |
Type: | North American TB-25N Mitchell |
Owner/operator: | Commemorative Air Force |
Registration: | N25YR |
MSN: | 43-27868 |
Year of manufacture: | 1943 |
Total airframe hrs: | 5231 hours |
Engine model: | Curtiss-Wright Cyclone |
Fatalities: | Fatalities: 0 / Occupants: 9 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | North of Dallas Executive Airport (KRBD), Dallas, TX -
United States of America
|
Phase: | Landing |
Nature: | Demo/Airshow/Display |
Departure airport: | Dallas, TX (RBD) |
Destination airport: | Dallas, TX (RBD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airline transport pilot reported that the twin-engine, historic airplane was flying about 155 mph and 1,000 ft above ground level. Upon entering the left downwind leg of the airport traffic pattern, the pilot extended the landing gear. While the gear was in transit, the crew felt a jolt, as if a bird had impacted the front of the airplane. The pilot made a normal landing, parked the airplane, and noted damage to the left horizontal stabilizer and elevator.
A crew from another airplane reported to the pilot that they observed an object depart the accident airplane during landing gear extension. A postaccident examination revealed that the left inboard landing gear door separated in flight and impacted the engine nacelle, left horizontal stabilizer, and elevator. The landing gear door was later found in a residential neighborhood about one mile north of the airport. The gear door was equipped with two arresting cables that were intended to prevent the door from hyperextending. The arresting cables were not installed in the correct position, and the investigation could not determine how long the arresting cables had been incorrectly installed. The landing gear door connecting rod was bent and fractured into two pieces at the safety wire drill hole. The fractured connecting rod was consistent with an overstress failure in bending. If the arresting cables had been installed correctly, it is likely that the landing gear door would not have separated from the airplane when the connecting rod failed.
Probable Cause: The overstress failure of the landing gear connecting rod and the improper installation of the arresting cables, which allowed the landing gear door to depart in flight and impact the airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN17LA033 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB
FAA register:
http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N25YR Location
Revision history:
Date/time | Contributor | Updates |
01-Nov-2016 20:53 |
Geno |
Added |
01-Nov-2016 20:58 |
Geno |
Updated [Operator] |
08-Sep-2017 19:48 |
ASN Update Bot |
Updated [Time, Operator, Total occupants, Nature, Departure airport, Destination airport, Source, Damage, Narrative] |
05-Nov-2017 08:46 |
ASN Update Bot |
Updated [Source, Narrative] |
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