Accident North American TB-25N Mitchell N25YR,
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ASN Wikibase Occurrence # 191041
 
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Date:Saturday 29 October 2016
Time:15:40
Type:Silhouette image of generic B25 model; specific model in this crash may look slightly different    
North American TB-25N Mitchell
Owner/operator:Commemorative Air Force
Registration: N25YR
MSN: 43-27868
Year of manufacture:1943
Total airframe hrs:5231 hours
Engine model:Curtiss-Wright Cyclone
Fatalities:Fatalities: 0 / Occupants: 9
Aircraft damage: Substantial
Category:Accident
Location:North of Dallas Executive Airport (KRBD), Dallas, TX -   United States of America
Phase: Landing
Nature:Demo/Airshow/Display
Departure airport:Dallas, TX (RBD)
Destination airport:Dallas, TX (RBD)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airline transport pilot reported that the twin-engine, historic airplane was flying about 155 mph and 1,000 ft above ground level. Upon entering the left downwind leg of the airport traffic pattern, the pilot extended the landing gear. While the gear was in transit, the crew felt a jolt, as if a bird had impacted the front of the airplane. The pilot made a normal landing, parked the airplane, and noted damage to the left horizontal stabilizer and elevator.

A crew from another airplane reported to the pilot that they observed an object depart the accident airplane during landing gear extension. A postaccident examination revealed that the left inboard landing gear door separated in flight and impacted the engine nacelle, left horizontal stabilizer, and elevator. The landing gear door was later found in a residential neighborhood about one mile north of the airport. The gear door was equipped with two arresting cables that were intended to prevent the door from hyperextending. The arresting cables were not installed in the correct position, and the investigation could not determine how long the arresting cables had been incorrectly installed. The landing gear door connecting rod was bent and fractured into two pieces at the safety wire drill hole. The fractured connecting rod was consistent with an overstress failure in bending. If the arresting cables had been installed correctly, it is likely that the landing gear door would not have separated from the airplane when the connecting rod failed.
Probable Cause: The overstress failure of the landing gear connecting rod and the improper installation of the arresting cables, which allowed the landing gear door to depart in flight and impact the airplane.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CEN17LA033
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N25YR

Location

Revision history:

Date/timeContributorUpdates
01-Nov-2016 20:53 Geno Added
01-Nov-2016 20:58 Geno Updated [Operator]
08-Sep-2017 19:48 ASN Update Bot Updated [Time, Operator, Total occupants, Nature, Departure airport, Destination airport, Source, Damage, Narrative]
05-Nov-2017 08:46 ASN Update Bot Updated [Source, Narrative]

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