Loss of control Accident Beechcraft 36 Bonanza N3089A,
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ASN Wikibase Occurrence # 191252
 
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Date:Wednesday 9 November 2016
Time:13:30
Type:Silhouette image of generic BE36 model; specific model in this crash may look slightly different    
Beechcraft 36 Bonanza
Owner/operator:Private
Registration: N3089A
MSN: E-182
Year of manufacture:1969
Total airframe hrs:5886 hours
Engine model:Continental IO-520-BA6B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Plantation Bay, Volusia-Flagler County, FL -   United States of America
Phase: En route
Nature:Private
Departure airport:Palm Coast, FL (KFIN)
Destination airport:Deland, FL (KDED)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The private pilot and the pilot-rated passenger reported that, while in level flight at an altitude of 2,000 ft mean sea level with the autopilot disengaged, the airplane suddenly rolled to the right without any control input. The pilot stated that he tried to correct with opposite aileron, but the airplane did not respond and continued to roll inverted. The pilot-rated passenger then took control of the airplane, shut off the engine, and applied full left rudder to bring the airplane back to level flight; however, the airplane had descended to about 300 ft. The pilot-rated passenger slowed the airplane and flared it into trees. The pilot stated that he had no idea what caused the airplane to suddenly roll, that the ailerons were unresponsive, and that he assumed a flight control cable had “snapped.” The pilot-rated passenger stated that they were not trying to perform aerobatics and that he thought the airplane rolled due to a broken aileron cable. 
Examination of the accident site revealed that the airplane first struck a 30- to 40-ft-tall tree with its right wing, then struck a second tree with the right wing. A 9-ft-long section of the right wing separated from the airplane and was found at the base of the second tree. Examination of the wreckage revealed that the right aileron UP flight control cable was separated at the turnbuckle, which was located inside the cabin, and the aileron balance control cable was separated in the right wing. Metallurgical examination of the cables revealed that they had both separated from overstress, indicative of the cables separating during the accident sequence. Examination of the airplane’s flight controls did not otherwise reveal any evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation.



Probable Cause: A loss of aircraft control for reasons that could not be determined because postaccident examination did not reveal any evidence of preimpact mechanical malfunctions or failures of the flight controls that would have precluded normal operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ERA17LA041
Status: Investigation completed
Duration: 2 years and 4 months
Download report: Final report

Sources:

NTSB
FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=N3089A

History of this aircraft

Other occurrences involving this aircraft
13 November 1999 N3089A B A D Aero Inc 0 Daytona Beach, FL sub

Location

Images:


Photo: NTSB

Media:

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Revision history:

Date/timeContributorUpdates
09-Nov-2016 20:39 Iceman 29 Added
10-Nov-2016 00:32 Geno Updated [Time, Aircraft type, Registration, Cn, Operator, Nature, Departure airport, Destination airport, Source, Embed code]
10-Nov-2016 14:06 Iceman 29 Updated [Embed code]
19-Nov-2016 12:28 Aerossurance Updated [Time, Location]
22-Mar-2019 19:08 ASN Update Bot Updated [Time, Aircraft type, Operator, Nature, Departure airport, Destination airport, Source, Embed code, Narrative, Accident report, ]
24-Mar-2019 08:33 harro Updated [Departure airport, Destination airport, Source, Embed code, Narrative, Photo]

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