ASN Wikibase Occurrence # 191494
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Date: | Sunday 6 June 2010 |
Time: | 14:40 |
Type: | P & M Quik R |
Owner/operator: | Private |
Registration: | G-CFTE |
MSN: | 8426 |
Year of manufacture: | 2008 |
Engine model: | Rotax 912ULS |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Destroyed |
Category: | Accident |
Location: | Oakley Airfield, Menmarsh Road, Worminghall, Aylesbury, Buckinghamshir -
United Kingdom
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Oakley Airfield, Aylesbury, Buckinghamshire |
Destination airport: | Oakley Airfield, Aylesbury, Buckinghamshire |
Investigating agency: | AAIB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Written off (damaged beyond repair) 06-06-2010 when crashed at Oakley Airfield, Menmarsh Road, Worminghall, Aylesbury, Buckinghamshire: The aircraft bounced on landing and subsequently stalled due to an excessive pitch attitude during an attempted go around. No injuries were reported to the two persons on board (pilot and one passenger). According to the following excerpt from the official AAIB report into the accident:
"The pilot had undertaken a local flight with a passenger and was returning to land at his departure airfield. A straight in approach was flown from a distance of about 3 nautical miles, but as he approached the threshold the pilot judged he was too high, so he closed the throttle.
The aircraft then sank, contacting the runway and bouncing. The pilot stated that he decided to go around and applied full power, at which point the aircraft stalled. The right wing dropped, inducing a turn to the right and, despite the efforts of the pilot to recover the aircraft attitude, it struck the ground again. The pilot closed the throttle and the aircraft rolled to a stop in an area of crops alongside the runway. Neither occupant was injured but the aircraft suffered damage to the base tube, front fork and right rear wheel.
The pilot stated that he reacted with appropriate speed in applying power after the aircraft bounced, but had not appreciated the high wing attitude and low airspeed, and did not attempt to adjust these sufficiently early to prevent the stall."
Nature of Damage sustained: Per the AAIB report "Damage to base tube, front fork and right main wheel". The damaged sustained was presumably enough to render the airframe as "beyond economic repair", as the registration G-CFTE was cancelled by the CAA on 14-03-2012 as "Permanently Withdrawn From Use"
Accident investigation:
|
| |
Investigating agency: | AAIB |
Report number: | EW/G2010/06/07 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
1. AAIB:
https://assets.publishing.service.gov.uk/media/5422f122e5274a1314000349/P_and_M_Quik_R__G-CFTE_02-11.pdf 2. CAA:
https://siteapps.caa.co.uk/g-info/ 3. G-CFTE P & M Aviation QuikR at Newtownards Airfield 23/05/09:
https://www.flickr.com/photos/ghbhd/14243743026/ 4.
https://www.bucks-microlight-club.org.uk/Airfield_Information/Airfield_info_example.html Revision history:
Date/time | Contributor | Updates |
20-Nov-2016 15:54 |
Dr.John Smith |
Added |
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