Accident Diamond DA40NG Diamond Star N605SJ,
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ASN Wikibase Occurrence # 192539
 
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Date:Thursday 29 December 2016
Time:13:30 LT
Type:Silhouette image of generic DA40 model; specific model in this crash may look slightly different    
Diamond DA40NG Diamond Star
Owner/operator:Ctc Aviation Leasing (us) Inc
Registration: N605SJ
MSN: 40.N284
Year of manufacture:2015
Total airframe hrs:1384 hours
Engine model:AUSTRO E4
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Mohave County north of Lake Havasu City, AZ -   United States of America
Phase: Landing
Nature:Private
Departure airport:Kingman, AZ (KIGM)
Destination airport:LAKE HAVASU CITY, AZ (HII
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that, during cruise flight, the airframe began to shake, and he received a failure annunciation indication from both engine control units, followed by indications of an increase in oil temperature and a loss of oil pressure. He decided to perform a forced landing into a field, during which both wings impacted vegetation and the airplane sustained substantial damage. Subsequent examination revealed that a large quantity of engine oil had been expelled out of the engine breather tube and onto the belly of the airplane.
Disassembly of the engine revealed heavy pitting to the piston crown and combustion chamber surfaces of the No. 1 cylinder. The damage appeared to be the result of a fatigue crack in the piston, which allowed combustion gases to create a gas path, which eventually tunneled through the piston. The path ultimately reached the lowest piston ring, allowing pressurization of the engine crankcase, resulting in the observed expulsion of oil.
The crack appeared to have been initiated by a nick in the piston crown, possibly caused by ingestion of a foreign wire-like object, which was harder than the aluminum material that comprised the piston and cylinder head.
A determination of the foreign object type could not be made, but there are multiple possibilities regarding the source. The induction side of the turbocharger had experienced a failure about 234 flight hours prior, and the induction-to-intake plenum was replaced 192 hours prior to the accident. A fragment of material, such as safety wire, could have been inadvertently left inside the unfiltered side of the induction system during those maintenance events and been ingested into the engine. The design of the air induction system incorporated filters for both normal and alternate air operations, and, as such, foreign object ingestion during operation was unlikely.
The engine's oil analysis history did not indicate any significant deviations throughout its service history. Such damage would likely have resulted in oil contamination; therefore, the crack likely began to propagate during the 90-hour period between the last oil analysis and the accident flight.
Multiple similar piston failures have occurred to other engines in the series, seemingly initiated by either foreign object ingestion and damage or thermal overload due to an out-of-tolerance fuel injector, or a combination of both.
The manufacturer released a mandatory service bulletin to address the fuel injector defects and a service letter to address the potential for foreign object ingestion following maintenance events.
Although not contributing to the accident, during the investigation, a series of cracks were observed in the cylinder head of both the accident engine and a series of other similar engines. In one event, a crack led to a loss of coolant after the cooling system became over-pressurized. In all cases, the cracks had occurred before the engines had reached their service life.
The FAA-certified engine was originally designed and manufactured for automobile use, and subsequently modified by the manufacturer for aviation use. As such, the engine was not operating in the manner (continuous high-power operation) for which it was originally designed. The significance of this finding could not be determined.

Probable Cause: The loss of engine oil pressure during cruise flight, which resulted in partial loss of engine power and necessitated a forced landing. The loss of oil pressure was the result of a failed engine piston, likely initiated by foreign object damage, which resulted in the pressurization of the crankcase and expulsion of the engine oil.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR17LA050
Status: Investigation completed
Duration: 4 years and 6 months
Download report: Final report

Sources:

NTSB WPR17LA050

FAA register: http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=605SJ

Location

Revision history:

Date/timeContributorUpdates
04-Jan-2017 02:37 Geno Added
29-Aug-2020 12:35 harro Updated [Narrative]
09-Jul-2022 12:50 ASN Update Bot Updated [Time, Operator, Total occupants, Other fatalities, Nature, Departure airport, Destination airport, Source, Damage, Narrative, Category, Accident report]

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