Accident investigation report completed and information captured
Narrative: Witnesses observed the airplane touch down left of the runway centerline in gusting crosswind conditions and then attempt to go-around. As the engine noise increased, the airplane yawed 90° left and banked left, perpendicular to the runway. The airplane's nose pitched up, and the airplane subsequently entered an aerodynamic stall and rolled inverted before impacting a ravine about 400 ft left of the runway. Examination of the wreckage did not reveal any preimpact mechanical malfunctions that would have precluded normal operation. The airplane was equipped with a 450-hp radial engine. It is likely that, upon application of engine power to initiate the go-around, the pilot failed to adequately compensate for the extreme left-turning tendencies of the high-powered engine, which resulted in a subsequent loss of control and aerodynamic stall. Probable Cause: The pilot's failure to maintain airplane control during an attempted go-around in gusting crosswind conditions, which resulted in an exceedance of the airplane's critical angle of attack and a subsequent aerodynamic stall.