| Date: | Friday 3 January 1964 |
| Time: | 11:00 |
| Type: | Beechcraft 35 Bonanza |
| Owner/operator: | Conatt Corp. |
| Registration: | N419B |
| MSN: | D-1425 |
| Year of manufacture: | 1948 |
| Fatalities: | Fatalities: 0 / Occupants: 2 |
| Other fatalities: | 0 |
| Aircraft damage: | Substantial |
| Category: | Accident |
| Location: | St.Paul, Minnesota -
United States of America
|
| Phase: | Take off |
| Nature: | Executive |
| Departure airport: | |
| Destination airport: | |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Gear retracted early & damaged on take-off, collapsed during taxi after landing.
Accident investigation:
|
|
| | |
| Investigating agency: | NTSB |
| Report number: | UNK64X0135 |
| Status: | Investigation completed |
| Duration: | |
| Download report: | Final report
|
|
Sources:
NTSB Identification:
Unknownhttp://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=82620&key=0http://www.ab-ix.co.uk/d-1000_to_d-1999.pdf
History of this aircraft
Other occurrences involving this aircraft Revision history:
| Date/time | Contributor | Updates |
The Aviation Safety Network is an exclusive service provided by:

CONNECT WITH US:
©2025 Flight Safety Foundation