ASN Wikibase Occurrence # 201955
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Date: | Friday 12 February 1999 |
Time: | 09:21 LT |
Type: | Cessna 210G |
Owner/operator: | Red Baron Aviation |
Registration: | N5874F |
MSN: | 21058874 |
Year of manufacture: | 1967 |
Total airframe hrs: | 12690 hours |
Engine model: | Continental IO-520-16B |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lake Placid, FL -
United States of America
|
Phase: | En route |
Nature: | Ferry/positioning |
Departure airport: | Brooksville, FL (XO5) |
Destination airport: | Opa Locka, FL (KOPF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The purpose of the flight was to position the airplane at the Miami's Opa Locka Airport. At an altitude of 5,000 feet agl under radar control, the pilot heard a 'snap/thud, followed by a popping noise,' and subsequent engine and propeller stoppage. An airborne restart was unsuccessful, and the propeller would not turn. The pilot realized he could not make it safely to an airport, and landed the airplane in a pasture. The airplane struck a tree, separating the left wing from the airframe. The nose and right main landing gear collided with a gully causing them to separate. According to the operator's records the subject engine was remanufactured by Continental Motors on December 9, 1997, and had 1622.9 hours of operating time since it was installed. The crankshaft was examined at the NTSB Materials Laboratory, and revealed that the crankshaft separated due to a fatigue crack that originated from the aft fillet radius of the No. 2 main journal. The fatigue area contained circumferential gouge marks and heat damage that was consistent with a bearing shell that had rotated or shifted. The bearing shell from the No. 1 rod journal also contained wear damage on the aft and forward edges that were consistent with shifting during engine operation.
Probable Cause: a total loss of engine power due to an in-flight separation of the crankshaft, caused by a fatigue crack that originated from the aft fillet radius of the No. 2 main journal, resulting in a forced landing in a field and impact with a tree.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA99LA081 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB MIA99LA081
Revision history:
Date/time | Contributor | Updates |
26-Nov-2017 10:00 |
ASN Update Bot |
Added |
08-Apr-2024 09:50 |
ASN Update Bot |
Updated [Time, Other fatalities, Phase, Destination airport, Source, Narrative, Accident report] |
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